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author | Andy Green <andy.green@txtr.com> | 2010-02-01 13:28:54 +0100 |
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committer | Sascha Hauer <s.hauer@pengutronix.de> | 2010-02-16 17:16:47 +0100 |
commit | 94d32f99c6aba8b702a9cf78cb328aeb7882b1e5 (patch) | |
tree | a3544b4959da6e325c11d9cd568b07bdd4c0a94c /arch/arm/mach-ebsa110 | |
parent | mx31moboard: support for the smartbot baseboard (diff) | |
download | linux-94d32f99c6aba8b702a9cf78cb328aeb7882b1e5.tar.xz linux-94d32f99c6aba8b702a9cf78cb328aeb7882b1e5.zip |
imx-serial-excessive-status-clearing-on-break.patch
cc: Sasha Hauer <kernel@pengutronix.de>
We noticed that we were only able to communicate once with a GSM module
per session, if we powered down the module then the serial driver was
broken until reset, no traffic or /proc/interrupts activity could be
seen any more.
Volker noticed it was provoked by a long "break" seen on the wire when
the RX was not driven during powerdown, we discovered we could kill the
serial driver just by forcing RX low extenally for a little while.
I saw that the processing for BREAK in the driver gets too excited and
clears down all set bits in USR2, including that a character is pending.
This stops all further characters getting processed.
The attached one-liner makes the serial driver immortal against BREAK.
Signed-off-by: Andy Green <andy.green@txtr.com>
Signed-off-by: Volker Ernst <volker.ernst@txtr.com>
Signed-off-by: Sascha Hauer <s.hauer@pengutronix.de>
Diffstat (limited to 'arch/arm/mach-ebsa110')
0 files changed, 0 insertions, 0 deletions