| Commit message (Collapse) | Author | Age | Files | Lines |
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There is a particular situation when the cooling device is cpufreq and the heat
dissipation is not efficient enough where the temperature increases little by
little until reaching the critical threshold and leading to a SoC reset.
The behavior is reproducible on a hikey6220 with bad heat dissipation (eg.
stacked with other boards).
Running a simple C program doing while(1); for each CPU of the SoC makes the
temperature to reach the passive regulation trip point and ends up to the
maximum allowed temperature followed by a reset.
This issue has been also reported by running the libhugetlbfs test suite.
What is observed is a ping pong between two cpu frequencies, 1.2GHz and 900MHz
while the temperature continues to grow.
It appears the step wise governor calls get_target_state() the first time with
the throttle set to true and the trend to 'raising'. The code selects logically
the next state, so the cpu frequency decreases from 1.2GHz to 900MHz, so far so
good. The temperature decreases immediately but still stays greater than the
trip point, then get_target_state() is called again, this time with the
throttle set to true *and* the trend to 'dropping'. From there the algorithm
assumes we have to step down the state and the cpu frequency jumps back to
1.2GHz. But the temperature is still higher than the trip point, so
get_target_state() is called with throttle=1 and trend='raising' again, we jump
to 900MHz, then get_target_state() is called with throttle=1 and
trend='dropping', we jump to 1.2GHz, etc ... but the temperature does not
stabilizes and continues to increase.
[ 237.922654] thermal thermal_zone0: Trip0[type=1,temp=65000]:trend=1,throttle=1
[ 237.922678] thermal thermal_zone0: Trip1[type=1,temp=75000]:trend=1,throttle=1
[ 237.922690] thermal cooling_device0: cur_state=0
[ 237.922701] thermal cooling_device0: old_target=0, target=1
[ 238.026656] thermal thermal_zone0: Trip0[type=1,temp=65000]:trend=2,throttle=1
[ 238.026680] thermal thermal_zone0: Trip1[type=1,temp=75000]:trend=2,throttle=1
[ 238.026694] thermal cooling_device0: cur_state=1
[ 238.026707] thermal cooling_device0: old_target=1, target=0
[ 238.134647] thermal thermal_zone0: Trip0[type=1,temp=65000]:trend=1,throttle=1
[ 238.134667] thermal thermal_zone0: Trip1[type=1,temp=75000]:trend=1,throttle=1
[ 238.134679] thermal cooling_device0: cur_state=0
[ 238.134690] thermal cooling_device0: old_target=0, target=1
In this situation the temperature continues to increase while the trend is
oscillating between 'dropping' and 'raising'. We need to keep the current state
untouched if the throttle is set, so the temperature can decrease or a higher
state could be selected, thus preventing this oscillation.
Keeping the next_target untouched when 'throttle' is true at 'dropping' time
fixes the issue.
The following traces show the governor does not change the next state if
trend==2 (dropping) and throttle==1.
[ 2306.127987] thermal thermal_zone0: Trip0[type=1,temp=65000]:trend=1,throttle=1
[ 2306.128009] thermal thermal_zone0: Trip1[type=1,temp=75000]:trend=1,throttle=1
[ 2306.128021] thermal cooling_device0: cur_state=0
[ 2306.128031] thermal cooling_device0: old_target=0, target=1
[ 2306.231991] thermal thermal_zone0: Trip0[type=1,temp=65000]:trend=2,throttle=1
[ 2306.232016] thermal thermal_zone0: Trip1[type=1,temp=75000]:trend=2,throttle=1
[ 2306.232030] thermal cooling_device0: cur_state=1
[ 2306.232042] thermal cooling_device0: old_target=1, target=1
[ 2306.335982] thermal thermal_zone0: Trip0[type=1,temp=65000]:trend=0,throttle=1
[ 2306.336006] thermal thermal_zone0: Trip1[type=1,temp=75000]:trend=0,throttle=1
[ 2306.336021] thermal cooling_device0: cur_state=1
[ 2306.336034] thermal cooling_device0: old_target=1, target=1
[ 2306.439984] thermal thermal_zone0: Trip0[type=1,temp=65000]:trend=2,throttle=1
[ 2306.440008] thermal thermal_zone0: Trip1[type=1,temp=75000]:trend=2,throttle=0
[ 2306.440022] thermal cooling_device0: cur_state=1
[ 2306.440034] thermal cooling_device0: old_target=1, target=0
[ ... ]
After a while, if the temperature continues to increase, the next state becomes
2 which is 720MHz on the hikey. That results in the temperature stabilizing
around the trip point.
[ 2455.831982] thermal thermal_zone0: Trip0[type=1,temp=65000]:trend=1,throttle=1
[ 2455.832006] thermal thermal_zone0: Trip1[type=1,temp=75000]:trend=1,throttle=0
[ 2455.832019] thermal cooling_device0: cur_state=1
[ 2455.832032] thermal cooling_device0: old_target=1, target=1
[ 2455.935985] thermal thermal_zone0: Trip0[type=1,temp=65000]:trend=0,throttle=1
[ 2455.936013] thermal thermal_zone0: Trip1[type=1,temp=75000]:trend=0,throttle=0
[ 2455.936027] thermal cooling_device0: cur_state=1
[ 2455.936040] thermal cooling_device0: old_target=1, target=1
[ 2456.043984] thermal thermal_zone0: Trip0[type=1,temp=65000]:trend=0,throttle=1
[ 2456.044009] thermal thermal_zone0: Trip1[type=1,temp=75000]:trend=0,throttle=0
[ 2456.044023] thermal cooling_device0: cur_state=1
[ 2456.044036] thermal cooling_device0: old_target=1, target=1
[ 2456.148001] thermal thermal_zone0: Trip0[type=1,temp=65000]:trend=1,throttle=1
[ 2456.148028] thermal thermal_zone0: Trip1[type=1,temp=75000]:trend=1,throttle=1
[ 2456.148042] thermal cooling_device0: cur_state=1
[ 2456.148055] thermal cooling_device0: old_target=1, target=2
[ 2456.252009] thermal thermal_zone0: Trip0[type=1,temp=65000]:trend=2,throttle=1
[ 2456.252041] thermal thermal_zone0: Trip1[type=1,temp=75000]:trend=2,throttle=0
[ 2456.252058] thermal cooling_device0: cur_state=2
[ 2456.252075] thermal cooling_device0: old_target=2, target=1
IOW, this change is needed to keep the state for a cooling device if the
temperature trend is oscillating while the temperature increases slightly.
Without this change, the situation above leads to a catastrophic crash by a
hardware reset on hikey. This issue has been reported to happen on an OMAP
dra7xx also.
Signed-off-by: Daniel Lezcano <daniel.lezcano@linaro.org>
Cc: Keerthy <j-keerthy@ti.com>
Cc: John Stultz <john.stultz@linaro.org>
Cc: Leo Yan <leo.yan@linaro.org>
Tested-by: Keerthy <j-keerthy@ti.com>
Reviewed-by: Keerthy <j-keerthy@ti.com>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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Use round up division to ensure the programmed value of threshold and the lag
are not less than what we set, and in order to keep the accuracy while using
round up division, the step value should be a rounded up value. There is
no need to use hisi_thermal_round_temp.
Signed-off-by: Kevin Wangtao <kevin.wangtao@linaro.org>
Tested-by: Daniel Lezcano <daniel.lezcano@linaro.org> # hikey6220
Signed-off-by: Daniel Lezcano <daniel.lezcano@linaro.org>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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The sensor's clock is enabled and disabled outside of the probe and
disable function. Moving the corresponding action in the
hisi_thermal_setup() and hisi_thermal_disable_sensor(), factors out
some lines of code and makes the code more symmetric.
Signed-off-by: Kevin Wangtao <kevin.wangtao@linaro.org>
Tested-by: Daniel Lezcano <daniel.lezcano@linaro.org> # hikey6220
Signed-off-by: Daniel Lezcano <daniel.lezcano@linaro.org>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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The mutex is used to protect against writes in the configuration register.
That happens at probe time, with no possible race yet.
Then when the module is unloaded and at suspend/resume.
When the module is unloaded, it is an userspace operation, thus via a process.
Suspending the system goes through the freezer to suspend all the tasks
synchronously before continuing. So it is not possible to hit the suspend ops
in this driver while we are unloading it.
The resume is the same situation than the probe.
In other words, even if there are several places where we write the
configuration register, there is no situation where we can write it at the same
time, so far as I can judge
Signed-off-by: Daniel Lezcano <daniel.lezcano@linaro.org>
Reviewed-by: Leo Yan <leo.yan@linaro.org>
Tested-by: Leo Yan <leo.yan@linaro.org>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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The presence of the thermal data pointer in the sensor structure has the unique
purpose of accessing the thermal data in the interrupt handler.
The sensor pointer is passed when registering the interrupt handler, replace the
cookie by the thermal data pointer, so the back pointer is no longer needed.
Signed-off-by: Daniel Lezcano <daniel.lezcano@linaro.org>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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There is no point to specify the temperature as long variable, the int is
enough.
Replace all long variables to int, so making the code consistent.
Signed-off-by: Daniel Lezcano <daniel.lezcano@linaro.org>
Reviewed-by: Leo Yan <leo.yan@linaro.org>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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Rename the 'sensors' field to 'sensor' as we describe only one sensor.
Remove the 'sensor_temp' as it is no longer used.
Signed-off-by: Daniel Lezcano <daniel.lezcano@linaro.org>
Reviewed-by: Leo Yan <leo.yan@linaro.org>
Tested-by: Leo Yan <leo.yan@linaro.org>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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The sensor is all setup, bind, resetted, acked, etc... every single second.
That was the way to workaround a problem with the interrupt bouncing again and
again.
With the following changes, we fix all in one:
- Do the setup, one time, at probe time
- Add the IRQF_ONESHOT, ack the interrupt in the threaded handler
- Remove the interrupt handler
- Set the correct value for the LAG register
- Remove all the irq_enabled stuff in the code as the interruption
handling is fixed
- Remove the 3ms delay
- Reorder the initialization routine to be in the right order
It ends up to a nicer code and more efficient, the 3-5ms delay is removed from
the get_temp() path.
Signed-off-by: Daniel Lezcano <daniel.lezcano@linaro.org>
Reviewed-by: Leo Yan <leo.yan@linaro.org>
Tested-by: Leo Yan <leo.yan@linaro.org>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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The TEMP0_CFG configuration register contains different field to set up the
temperature controller. However in the code, nothing prevents a setup to
overwrite the previous one: eg. writing the hdak value overwrites the sensor
selection, the sensor selection overwrites the hdak value.
In order to prevent such thing, use a regmap-like mechanism by reading the
value before, set the corresponding bits and write the result.
Signed-off-by: Daniel Lezcano <daniel.lezcano@linaro.org>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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Hopefully, the function name can help to clarify the semantic of the operations
when writing in the register.
Signed-off-by: Daniel Lezcano <daniel.lezcano@linaro.org>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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The threaded interrupt inspect the sensors structure to look in the temp
threshold field, but this field is read-only in all the code, except in the
probe function before the threaded interrupt is set. In other words there
is not race window in the threaded interrupt when reading the field value.
Signed-off-by: Daniel Lezcano <daniel.lezcano@linaro.org>
Reviewed-by: Leo Yan <leo.yan@linaro.org>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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The DT specifies a threshold of 65000, we setup the register with a value in
the temperature resolution for the controller, 64656.
When we reach 64656, the interrupt fires, the interrupt is disabled. Then the
irq thread runs and calls thermal_zone_device_update() which will call in turn
hisi_thermal_get_temp().
The function will look if the temperature decreased, assuming it was more than
65000, but that is not the case because the current temperature is 64656
(because of the rounding when setting the threshold). This condition being
true, we re-enable the interrupt which fires immediately after exiting the irq
thread. That happens again and again until the temperature goes to more than
65000.
Potentially, there is here an interrupt storm if the temperature stabilizes at
this temperature. A very unlikely case but possible.
In any case, it does not make sense to handle dozens of alarm interrupt for
nothing.
Fix this by rounding the threshold value to the controller resolution so the
check against the threshold is consistent with the one set in the controller.
Signed-off-by: Daniel Lezcano <daniel.lezcano@linaro.org>
Reviewed-by: Leo Yan <leo.yan@linaro.org>
Tested-by: Leo Yan <leo.yan@linaro.org>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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The step and the base temperature are fixed values, we can simplify the
computation by converting the base temperature to milli celsius and use a
pre-computed step value. That saves us a lot of mult + div for nothing at
runtime.
Take also the opportunity to change the function names to be consistent with
the rest of the code.
Signed-off-by: Daniel Lezcano <daniel.lezcano@linaro.org>
Reviewed-by: Leo Yan <leo.yan@linaro.org>
Tested-by: Leo Yan <leo.yan@linaro.org>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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The threaded interrupt for the alarm interrupt is requested before the
temperature controller is setup. This one can fire an interrupt immediately
leading to a kernel panic as the sensor data is not initialized.
In order to prevent that, move the threaded irq after the Tsensor is setup.
Signed-off-by: Daniel Lezcano <daniel.lezcano@linaro.org>
Reviewed-by: Leo Yan <leo.yan@linaro.org>
Tested-by: Leo Yan <leo.yan@linaro.org>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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By essence, the tsensor does not really support multiple sensor at the same
time. It allows to set a sensor and use it to get the temperature, another
sensor could be switched but with a delay of 3-5ms. It is difficult to read
simultaneously several sensors without a big delay.
Today, just one sensor is used, it is not necessary to deal with multiple
sensors in the code. Remove them and if it is needed in the future add them
on top of a code which will be clean up in the meantime.
Signed-off-by: Daniel Lezcano <daniel.lezcano@linaro.org>
Reviewed-by: Leo Yan <leo.yan@linaro.org>
Acked-by: Wangtao (Kevin, Kirin) <kevin.wangtao@hisilicon.com>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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The interrupt for the temperature threshold is not enabled at the end of the
probe function, enable it after the setup is complete.
On the other side, the irq_enabled is not correctly set as we are checking if
the interrupt is masked where 'yes' means irq_enabled=false.
irq_get_irqchip_state(data->irq, IRQCHIP_STATE_MASKED,
&data->irq_enabled);
As we are always enabling the interrupt, it is pointless to check if
the interrupt is masked or not, just set irq_enabled to 'true'.
Signed-off-by: Daniel Lezcano <daniel.lezcano@linaro.org>
Reviewed-by: Leo Yan <leo.yan@linaro.org>
Tested-by: Leo Yan <leo.yan@linaro.org>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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on unload
While debugging some PM issues and trying to remove all the loaded modules, I ran
across the following when unloading ti-soc-thermal:
Unable to handle kernel NULL pointer dereference at virtual address 000000b4
...
[<c08db340>] (kobject_put) from [<bf28954c>] (ti_thermal_unregister_cpu_cooling+0x20/0x28 [ti_soc_thermal])
[<bf28954c>] (ti_thermal_unregister_cpu_cooling [ti_soc_thermal]) from [<bf287c88>] (ti_bandgap_remove+0x3c/0x104 [ti_soc_thermal])
[<bf287c88>] (ti_bandgap_remove [ti_soc_thermal]) from [<c0610d48>] (platform_drv_remove+0x24/0x3c)
[<c0610d48>] (platform_drv_remove) from [<c060f114>] (device_release_driver_internal+0x160/0x208)
[<c060f114>] (device_release_driver_internal) from [<c060f200>] (driver_detach+0x38/0x6c)
[<c060f200>] (driver_detach) from [<c060e2d4>] (bus_remove_driver+0x4c/0xa0)
[<c060e2d4>] (bus_remove_driver) from [<c01f2370>] (SyS_delete_module+0x168/0x238)
[<c01f2370>] (SyS_delete_module) from [<c0108240>] (ret_fast_syscall+0x0/0x28)
Cc: Keerthy <j-keerthy@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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The initialization sequence for H3 (r8a7795) ES1.x and ES2.0 is
different. H3 ES2.0 and later uses the same sequence as M3 (r8a7796)
ES1.0. Fix this by not looking at compatible strings and instead
defaulting to the r8a7796 initialization sequence and use
soc_device_match() to check for H3 ES1.x.
Signed-off-by: Niklas Söderlund <niklas.soderlund+renesas@ragnatech.se>
Reviewed-by: Geert Uytterhoeven <geert+renesas@glider.be>
Acked-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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The formula implementation at armada_get_temp() indicates that the sign
in the formula is inverted.
Cc: Ezequiel Garcia <ezequiel@vanguardiasur.com.ar>
Signed-off-by: Baruch Siach <baruch@tkos.co.il>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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The dev pointer is going through a null check after a dereference.
So this patch removes that useless check since the driver does not
pass a null dev pointer in any case.
Signed-off-by: Nicolin Chen <nicoleotsuka@gmail.com>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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Moving the bcm2835 thermal driver to the broadcom directory prevented it
from getting enabled for arm64 builds, since the broadcom directory is only
available when 32-bit specific ARCH_BCM is set.
Fix this by enabling the Broadcom menu for ARCH_BCM or ARCH_BCM2835.
Fixes: 6892cf07e733 ("thermal: bcm2835: move to the broadcom subdirectory")
Reviewed-by: Eric Anholt <eric@anholt.net>
Signed-off-by: Allen Wild <allenwild93@gmail.com>
Signed-off-by: Stefan Wahren <stefan.wahren@i2se.com>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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RV1108 SOC has one Temperature Sensor for CPU.
Reviewed-by: Caesar Wang <wxt@rock-chips.com>
Signed-off-by: Rocky Hao <rocky.hao@rock-chips.com>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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Add a new compatible for thermal founding on RV1108 SoCs.
Acked-by: Rob Herring <robh@kernel.org>
Signed-off-by: Rocky Hao <rocky.hao@rock-chips.com>
Signed-off-by: Eduardo Valentin <edubezval@gmail.com>
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Pull UBI updates from Richard Weinberger:
"Minor improvements"
* tag 'upstream-4.14-rc1' of git://git.infradead.org/linux-ubifs:
UBI: Fix two typos in comments
ubi: fastmap: fix spelling mistake: "invalidiate" -> "invalidate"
ubi: pr_err() strings should end with newlines
ubi: pr_err() strings should end with newlines
ubi: pr_err() strings should end with newlines
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Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Richard Weinberger <richard@nod.at>
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Trivial fix to spelling mistake in ubi_err error message
Signed-off-by: Colin Ian King <colin.king@canonical.com>
Reviewed-by: Boris Brezillon <boris.brezillon@free-electrons.com>
Signed-off-by: Richard Weinberger <richard@nod.at>
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In build.c, the following pr_err calls should be terminated with
a new-line to avoid other messages being concatenated onto the end.
Signed-off-by: Ben Dooks <ben.dooks@codethink.co.uk>
Signed-off-by: Richard Weinberger <richard@nod.at>
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In ubi_attach_mtd_dev() the pr_err() calls should have their
messgaes terminated with a new-line to avoid other messages
being concatenated onto the end.
Signed-off-by: Ben Dooks <ben.dooks@codethink.co.uk>
Signed-off-by: Richard Weinberger <richard@nod.at>
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The ubi_init() function has a few error paths that use the
pr_err() to output errors. These should have new lines on
them as pr_err() does not automatically do this.
This fixes issues where if multiple mtd fail to bind to
ubi the console output starts wrapping around.
Signed-off-by: Ben Dooks <ben.dooks@codethink.co.uk>
Signed-off-by: Richard Weinberger <richard@nod.at>
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git://git.kernel.org/pub/scm/linux/kernel/git/rw/uml
Pull UML updates from Richard Weinberger:
- minor improvements
- fixes for Debian's new gcc defaults (pie enabled by default)
- fixes for XSTATE/XSAVE to make UML work again on modern systems
* 'for-linus-4.14-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/rw/uml:
um: return negative in tuntap_open_tramp()
um: remove a stray tab
um: Use relative modversions with LD_SCRIPT_DYN
um: link vmlinux with -no-pie
um: Fix CONFIG_GCOV for modules.
Fix minor typos and grammar in UML start_up help
um: defconfig: Cleanup from old Kconfig options
um: Fix FP register size for XSTATE/XSAVE
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The intention is to return negative error codes. "pid" is already
negative but we accidentally negate it again back to positive.
Signed-off-by: Dan Carpenter <dan.carpenter@oracle.com>
Signed-off-by: Richard Weinberger <richard@nod.at>
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Static checkers would urge us to add curly braces to this code, but
actually the code works correctly. It just isn't indented right.
Signed-off-by: Dan Carpenter <dan.carpenter@oracle.com>
Signed-off-by: Richard Weinberger <richard@nod.at>
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When building a dynamic kernel image use relative symbols with MODVERSIONS.
Signed-off-by: Thomas Meyer <thomas@m3y3r.de>
Signed-off-by: Richard Weinberger <richard@nod.at>
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Debian's gcc defaults to pie. The global Makefile already defines the -fno-pie option.
Link UML dynamic kernel image also with -no-pie to fix the build.
Signed-off-by: Thomas Meyer <thomas@m3y3r.de>
Signed-off-by: Richard Weinberger <richard@nod.at>
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Explicitly export symbols so modpost doesn't complain.
Signed-off-by: Thomas Meyer <thomas@m3y3r.de>
Signed-off-by: Richard Weinberger <richard@nod.at>
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Signed-off-by: James Pack <jpack61108@gmail.com>
Signed-off-by: Richard Weinberger <richard@nod.at>
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Remove old, dead Kconfig option INET_LRO. It is gone since
commit 7bbf3cae65b6 ("ipv4: Remove inet_lro library").
Signed-off-by: Krzysztof Kozlowski <krzk@kernel.org>
Signed-off-by: Richard Weinberger <richard@nod.at>
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Hard code max size. Taken from
https://sourceware.org/git/?p=binutils-gdb.git;a=blob;f=gdb/common/x86-xstate.h
Signed-off-by: Thomas Meyer <thomas@m3y3r.de>
Signed-off-by: Richard Weinberger <richard@nod.at>
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Pull networking fixes from David Miller:
1) Fix hotplug deadlock in hv_netvsc, from Stephen Hemminger.
2) Fix double-free in rmnet driver, from Dan Carpenter.
3) INET connection socket layer can double put request sockets, fix
from Eric Dumazet.
4) Don't match collect metadata-mode tunnels if the device is down,
from Haishuang Yan.
5) Do not perform TSO6/GSO on ipv6 packets with extensions headers in
be2net driver, from Suresh Reddy.
6) Fix scaling error in gen_estimator, from Eric Dumazet.
7) Fix 64-bit statistics deadlock in systemport driver, from Florian
Fainelli.
8) Fix use-after-free in sctp_sock_dump, from Xin Long.
9) Reject invalid BPF_END instructions in verifier, from Edward Cree.
* git://git.kernel.org/pub/scm/linux/kernel/git/davem/net: (43 commits)
mlxsw: spectrum_router: Only handle IPv4 and IPv6 events
Documentation: link in networking docs
tcp: fix data delivery rate
bpf/verifier: reject BPF_ALU64|BPF_END
sctp: do not mark sk dumped when inet_sctp_diag_fill returns err
sctp: fix an use-after-free issue in sctp_sock_dump
netvsc: increase default receive buffer size
tcp: update skb->skb_mstamp more carefully
net: ipv4: fix l3slave check for index returned in IP_PKTINFO
net: smsc911x: Quieten netif during suspend
net: systemport: Fix 64-bit stats deadlock
net: vrf: avoid gcc-4.6 warning
qed: remove unnecessary call to memset
tg3: clean up redundant initialization of tnapi
tls: make tls_sw_free_resources static
sctp: potential read out of bounds in sctp_ulpevent_type_enabled()
MAINTAINERS: review Renesas DT bindings as well
net_sched: gen_estimator: fix scaling error in bytes/packets samples
nfp: wait for the NSP resource to appear on boot
nfp: wait for board state before talking to the NSP
...
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The driver doesn't support events from address families other than IPv4
and IPv6, so ignore them. Otherwise, we risk queueing a work item before
it's initialized.
This can happen in case a VRF is configured when MROUTE_MULTIPLE_TABLES
is enabled, as the VRF driver will try to add an l3mdev rule for the
IPMR family.
Fixes: 65e65ec137f4 ("mlxsw: spectrum_router: Don't ignore IPv6 notifications")
Signed-off-by: Ido Schimmel <idosch@mellanox.com>
Reported-by: Andreas Rammhold <andreas@rammhold.de>
Reported-by: Florian Klink <flokli@flokli.de>
Signed-off-by: Jiri Pirko <jiri@mellanox.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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Fix link in filter.txt.
Acked-by: Pavel Machek <pavel@ucw.cz>
Signed-off-by: David S. Miller <davem@davemloft.net>
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Now skb->mstamp_skb is updated later, we also need to call
tcp_rate_skb_sent() after the update is done.
Fixes: 8c72c65b426b ("tcp: update skb->skb_mstamp more carefully")
Signed-off-by: Eric Dumazet <edumazet@google.com>
Acked-by: Soheil Hassas Yeganeh <soheil@google.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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Neither ___bpf_prog_run nor the JITs accept it.
Also adds a new test case.
Fixes: 17a5267067f3 ("bpf: verifier (add verifier core)")
Signed-off-by: Edward Cree <ecree@solarflare.com>
Acked-by: Alexei Starovoitov <ast@kernel.org>
Acked-by: Daniel Borkmann <daniel@iogearbox.net>
Signed-off-by: David S. Miller <davem@davemloft.net>
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sctp_diag would not actually dump out sk/asoc if inet_sctp_diag_fill
returns err, in which case it shouldn't mark sk dumped by setting
cb->args[3] as 1 in sctp_sock_dump().
Otherwise, it could cause some asocs to have no parent's sk dumped
in 'ss --sctp'.
So this patch is to not set cb->args[3] when inet_sctp_diag_fill()
returns err in sctp_sock_dump().
Fixes: 8f840e47f190 ("sctp: add the sctp_diag.c file")
Signed-off-by: Xin Long <lucien.xin@gmail.com>
Acked-by: Marcelo Ricardo Leitner <marcelo.leitner@gmail.com>
Acked-by: Neil Horman <nhorman@tuxdriver.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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Commit 86fdb3448cc1 ("sctp: ensure ep is not destroyed before doing the
dump") tried to fix an use-after-free issue by checking !sctp_sk(sk)->ep
with holding sock and sock lock.
But Paolo noticed that endpoint could be destroyed in sctp_rcv without
sock lock protection. It means the use-after-free issue still could be
triggered when sctp_rcv put and destroy ep after sctp_sock_dump checks
!ep, although it's pretty hard to reproduce.
I could reproduce it by mdelay in sctp_rcv while msleep in sctp_close
and sctp_sock_dump long time.
This patch is to add another param cb_done to sctp_for_each_transport
and dump ep->assocs with holding tsp after jumping out of transport's
traversal in it to avoid this issue.
It can also improve sctp diag dump to make it run faster, as no need
to save sk into cb->args[5] and keep calling sctp_for_each_transport
any more.
This patch is also to use int * instead of int for the pos argument
in sctp_for_each_transport, which could make postion increment only
in sctp_for_each_transport and no need to keep changing cb->args[2]
in sctp_sock_filter and sctp_sock_dump any more.
Fixes: 86fdb3448cc1 ("sctp: ensure ep is not destroyed before doing the dump")
Reported-by: Paolo Abeni <pabeni@redhat.com>
Signed-off-by: Xin Long <lucien.xin@gmail.com>
Acked-by: Marcelo Ricardo Leitner <marcelo.leitner@gmail.com>
Acked-by: Neil Horman <nhorman@tuxdriver.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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The default receive buffer size was reduced by recent change
to a value which was appropriate for 10G and Windows Server 2016.
But the value is too small for full performance with 40G on Azure.
Increase the default back to maximum supported by host.
Fixes: 8b5327975ae1 ("netvsc: allow controlling send/recv buffer size")
Signed-off-by: Stephen Hemminger <sthemmin@microsoft.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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liujian reported a problem in TCP_USER_TIMEOUT processing with a patch
in tcp_probe_timer() :
https://www.spinics.net/lists/netdev/msg454496.html
After investigations, the root cause of the problem is that we update
skb->skb_mstamp of skbs in write queue, even if the attempt to send a
clone or copy of it failed. One reason being a routing problem.
This patch prevents this, solving liujian issue.
It also removes a potential RTT miscalculation, since
__tcp_retransmit_skb() is not OR-ing TCP_SKB_CB(skb)->sacked with
TCPCB_EVER_RETRANS if a failure happens, but skb->skb_mstamp has
been changed.
A future ACK would then lead to a very small RTT sample and min_rtt
would then be lowered to this too small value.
Tested:
# cat user_timeout.pkt
--local_ip=192.168.102.64
0 socket(..., SOCK_STREAM, IPPROTO_TCP) = 3
+0 setsockopt(3, SOL_SOCKET, SO_REUSEADDR, [1], 4) = 0
+0 bind(3, ..., ...) = 0
+0 listen(3, 1) = 0
+0 `ifconfig tun0 192.168.102.64/16; ip ro add 192.0.2.1 dev tun0`
+0 < S 0:0(0) win 0 <mss 1460>
+0 > S. 0:0(0) ack 1 <mss 1460>
+.1 < . 1:1(0) ack 1 win 65530
+0 accept(3, ..., ...) = 4
+0 setsockopt(4, SOL_TCP, TCP_USER_TIMEOUT, [3000], 4) = 0
+0 write(4, ..., 24) = 24
+0 > P. 1:25(24) ack 1 win 29200
+.1 < . 1:1(0) ack 25 win 65530
//change the ipaddress
+1 `ifconfig tun0 192.168.0.10/16`
+1 write(4, ..., 24) = 24
+1 write(4, ..., 24) = 24
+1 write(4, ..., 24) = 24
+1 write(4, ..., 24) = 24
+0 `ifconfig tun0 192.168.102.64/16`
+0 < . 1:2(1) ack 25 win 65530
+0 `ifconfig tun0 192.168.0.10/16`
+3 write(4, ..., 24) = -1
# ./packetdrill user_timeout.pkt
Signed-off-by: Eric Dumazet <edumazet@googl.com>
Reported-by: liujian <liujian56@huawei.com>
Acked-by: Neal Cardwell <ncardwell@google.com>
Acked-by: Yuchung Cheng <ycheng@google.com>
Acked-by: Soheil Hassas Yeganeh <soheil@google.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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rt_iif is only set to the actual egress device for the output path. The
recent change to consider the l3slave flag when returning IP_PKTINFO
works for local traffic (the correct device index is returned), but it
broke the more typical use case of packets received from a remote host
always returning the VRF index rather than the original ingress device.
Update the fixup to consider l3slave and rt_iif actually getting set.
Fixes: 1dfa76390bf05 ("net: ipv4: add check for l3slave for index returned in IP_PKTINFO")
Signed-off-by: David Ahern <dsahern@gmail.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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If the network interface is kept running during suspend, the net core
may call net_device_ops.ndo_start_xmit() while the Ethernet device is
still suspended, which may lead to a system crash.
E.g. on sh73a0/kzm9g and r8a73a4/ape6evm, the external Ethernet chip is
driven by a PM controlled clock. If the Ethernet registers are accessed
while the clock is not running, the system will crash with an imprecise
external abort.
As this is a race condition with a small time window, it is not so easy
to trigger at will. Using pm_test may increase your chances:
# echo 0 > /sys/module/printk/parameters/console_suspend
# echo platform > /sys/power/pm_test
# echo mem > /sys/power/state
To fix this, make sure the network interface is quietened during
suspend.
Signed-off-by: Geert Uytterhoeven <geert+renesas@glider.be>
Reviewed-by: Florian Fainelli <f.fainelli@gmail.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
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