| Commit message (Collapse) | Author | Age | Files | Lines |
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There are two separate flags controlling whether or not the MPIC is
reset during initialization, which is completely unnecessary, and only
one of them can be specified in the device tree.
Also, most platforms in-tree right now do actually want to reset the
MPIC during initialization anyways, which means lots of duplicate code
passing the MPIC_WANTS_RESET flag.
Fix all of the callers which currently do not pass the MPIC_WANTS_RESET
flag to pass the MPIC_NO_RESET flag, then remove the MPIC_WANTS_RESET
flag and make the code reset the MPIC by default.
Signed-off-by: Kyle Moffett <Kyle.D.Moffett@boeing.com>
Signed-off-by: Benjamin Herrenschmidt <benh@kernel.crashing.org>
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The FreeScale PowerQUICC-III-compatible (mpc85xx/mpc86xx) MPICs do not
correctly report the number of hardware interrupt sources, so software
needs to override the detected value with "256".
To avoid needing to write custom board-specific code to detect that
scenario, allow it to be easily overridden in the device-tree.
Signed-off-by: Kyle Moffett <Kyle.D.Moffett@boeing.com>
Signed-off-by: Benjamin Herrenschmidt <benh@kernel.crashing.org>
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The mpic->irq_count variable is only used as a software error-checking
limit to determine whether or not an IRQ number is valid. In board code
which does not manually specify an IRQ count to mpic_alloc(), i.e. 0, it
is automatically detected from the number of ISUs and the ISU size.
In practice, all hardware ends up with irq_count == num_sources, so all
of the runtime checks on mpic->irq_count should just check the value of
mpic->num_sources instead.
When platform hardware does not correctly report the number of IRQs,
which only happens on the MPC85xx/MPC86xx, the MPIC_BROKEN_FRR_NIRQS
flag is used to override the detected value of num_sources with the
manual irq_count parameter. Since there's no need to manually specify
the number of IRQs except in this case, the extra flag can be eliminated
and the test changed to "irq_count != 0".
Signed-off-by: Kyle Moffett <Kyle.D.Moffett@boeing.com>
Signed-off-by: Benjamin Herrenschmidt <benh@kernel.crashing.org>
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The Freescale MPIC (and perhaps others in the future) is incapable of
routing non-IPI interrupts to more than once CPU at a time. Currently
all of the Freescale boards msut pass the MPIC_SINGLE_DEST_CPU flag to
mpic_alloc(), but that information should really be present in the
device-tree.
Older board code can't rely on the device-tree having the property set,
but newer platforms won't need it manually specified in the code.
[BenH: Remove unrelated changes, folded in a different patch]
Signed-off-by: Kyle Moffett <Kyle.D.Moffett@boeing.com>
Signed-off-by: Benjamin Herrenschmidt <benh@kernel.crashing.org>
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The MPIC code checks for a "big-endian" property and sets the flag
MPIC_BIG_ENDIAN if one is present, although prior to the "mpic->flags"
fixup that would never have worked anways.
Unfortunately, even now that it works properly, the Freescale mpic
device-node (the "PowerQUICC-III"-compatible one) does not specify it,
so all of the board ports need to manually pass it to mpic_alloc().
Document the flag and add it to the pq3 device tree. Existing code will
still need to pass the MPIC_BIG_ENDIAN flag because their dtb may not
have this property, but new platforms shouldn't need to do so.
Signed-off-by: Kyle Moffett <Kyle.D.Moffett@boeing.com>
Signed-off-by: Benjamin Herrenschmidt <benh@kernel.crashing.org>
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The mpic_alloc() function takes a "flags" parameter and assigns it into
the mpic->flags variable fairly early on, but several later pieces of
code detect various device-tree properties and save them into the
"mpic->flags" variable (EG: "big-endian" => MPIC_BIG_ENDIAN).
Unfortunately, a number of codepaths (including several which test the
flag MPIC_BIG_ENDIAN!) test "flags" instead of "mpic->flags", and get
wrong answers as a result.
Consolidate the device-tree flag tests early in mpic_alloc() and change
all of the checks after "mpic->flags" is init'ed to use "mpic->flags".
[BenH: Fixed up use of mpic->node before it's initialized]
Signed-off-by: Kyle Moffett <Kyle.D.Moffett@boeing.com>
Signed-off-by: Benjamin Herrenschmidt <benh@kernel.crashing.org>
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(And define it properly for x86-32, which had its 'current_task'
declaration in separate from x86-64)
Bitten by my dislike for modules on the machines I use, and the fact
that apparently nobody else actually wanted to test the patches I sent
out.
Snif. Nobody else cares.
Anyway, we probably should uninline the 'kernel_fpu_begin()' function
that is what modules actually use and that references this, but this is
the minimal fix for now.
Reported-by: Josh Boyer <jwboyer@gmail.com>
Reported-and-tested-by: Jongman Heo <jongman.heo@samsung.com>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
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git://git.kernel.org/pub/scm/linux/kernel/git/s390/linux
* 'for-linus' of git://git.kernel.org/pub/scm/linux/kernel/git/s390/linux:
[S390] correct ktime to tod clock comparator conversion
[S390] 3215 deadlock with tty_wakeup
[S390] incorrect PageTables counter for kvm page tables
[S390] idle: avoid RCU usage in extended quiescent state
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The conversion of the ktime to a value suitable for the clock comparator
does not take changes to wall_to_monotonic into account. In fact the
conversion just needs the boot clock (sched_clock_base_cc) and the
total_sleep_time.
This is applicable to 3.2+ kernels.
CC: stable@vger.kernel.org
Signed-off-by: Martin Schwidefsky <schwidefsky@de.ibm.com>
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The page_table_free_pgste function is used for kvm processes to free page
tables that have the pgste extension. It calls pgtable_page_ctor instead of
pgtable_page_dtor which increases NR_PAGETABLE instead of decreasing it.
Signed-off-by: Martin Schwidefsky <schwidefsky@de.ibm.com>
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Avoid calling wake_up() from our NMI "bottom halve" from RCU extended
quiescent state in idle. wake_up() has RCU read-side critical sections
but this will be completely ignored by RCU if the cpu is in extended
quiescent state.
Which means that whatever object is being accessed from within the
read-side critical section can be freed concurrently from a different
cpu.
So make sure we leave extended quiescent state before calling wake_up().
Signed-off-by: Heiko Carstens <heiko.carstens@de.ibm.com>
Signed-off-by: Martin Schwidefsky <schwidefsky@de.ibm.com>
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This makes us recognize when we try to restore FPU state that matches
what we already have in the FPU on this CPU, and avoids the restore
entirely if so.
To do this, we add two new data fields:
- a percpu 'fpu_owner_task' variable that gets written any time we
update the "has_fpu" field, and thus acts as a kind of back-pointer
to the task that owns the CPU. The exception is when we save the FPU
state as part of a context switch - if the save can keep the FPU
state around, we leave the 'fpu_owner_task' variable pointing at the
task whose FP state still remains on the CPU.
- a per-thread 'last_cpu' field, that indicates which CPU that thread
used its FPU on last. We update this on every context switch
(writing an invalid CPU number if the last context switch didn't
leave the FPU in a lazily usable state), so we know that *that*
thread has done nothing else with the FPU since.
These two fields together can be used when next switching back to the
task to see if the CPU still matches: if 'fpu_owner_task' matches the
task we are switching to, we know that no other task (or kernel FPU
usage) touched the FPU on this CPU in the meantime, and if the current
CPU number matches the 'last_cpu' field, we know that this thread did no
other FP work on any other CPU, so the FPU state on the CPU must match
what was saved on last context switch.
In that case, we can avoid the 'f[x]rstor' entirely, and just clear the
CR0.TS bit.
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
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This inlines what is usually just a couple of instructions, but more
importantly it also fixes the theoretical error case (can that FPU
restore really ever fail? Maybe we should remove the checking).
We can't start sending signals from within the scheduler, we're much too
deep in the kernel and are holding the runqueue lock etc. So don't
bother even trying.
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
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This makes sure we clear the FPU usage counter for newly created tasks,
just so that we start off in a known state (for example, don't try to
preload the FPU state on the first task switch etc).
It also fixes a thinko in when we increment the fpu_counter at task
switch time, introduced by commit 34ddc81a230b ("i387: re-introduce FPU
state preloading at context switch time"). We should increment the
*new* task fpu_counter, not the old task, and only if we decide to use
that state (whether lazily or preloaded).
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
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git://git.kernel.org/pub/scm/linux/kernel/git/arm/arm-soc
These are the bug fixes that have accumulated since 3.3-rc3 in arm-soc.
The majority of them are regression fixes for stuff that broke during
the merge 3.3 window.
The notable ones are:
* The at91 ata drivers both broke because of an earlier cleanup patch that
some other patches were based on. Jean-Christophe decided to remove
the legacy at91_ide driver and fix the new-style at91-pata driver while
keeping the cleanup patch. I almost rejected the patches for being too
late and too big but in the end decided to accept them because they
fix a regression.
* A patch fixing build breakage from the sysdev-to-device conversion
colliding with other changes touches a number of mach-s3c files.
* b0654037 "ARM: orion: Fix Orion5x GPIO regression from MPP cleanup"
is a mechanical change that unfortunately touches a lot of lines
that should up in the diffstat.
* tag 'fixes-3.3-rc4' of git://git.kernel.org/pub/scm/linux/kernel/git/arm/arm-soc: (28 commits)
ARM: at91: drop ide driver in favor of the pata one
pata/at91: use newly introduced SMC accessors
ARM: at91: add accessor to manage SMC
ARM: at91:rtc/rtc-at91sam9: ioremap register bank
ARM: at91: USB AT91 gadget registration for module
ep93xx: fix build of vision_ep93xx.c
ARM: OMAP2xxx: PM: fix OMAP2xxx-specific UART idle bug in v3.3
ARM: orion: Fix USB phy for orion5x.
ARM: orion: Fix Orion5x GPIO regression from MPP cleanup
ARM: EXYNOS: Add cpu-offset property in gic device tree node
ARM: EXYNOS: Bring exynos4-dt up to date
ARM: OMAP3: cm-t35: fix section mismatch warning
ARM: OMAP2: Fix the OMAP2 only build break seen with 2011+ ARM tool-chains
ARM: tegra: paz00: fix wrong UART port on mini-pcie plug
ARM: tegra: paz00: fix wrong SD1 power gpio
i2c: tegra: Add devexit_p() for remove
ARM: EXYNOS: Correct M-5MOLS sensor clock frequency on Universal C210 board
ARM: EXYNOS: Correct framebuffer window size on Nuri board
ARM: SAMSUNG: Fix missing api-change from subsys_interface change
ARM: EXYNOS: Fix "warning: initialization from incompatible pointer type"
...
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* 'at91-fixes' of git://github.com/at91linux/linux-at91:
ARM: at91: drop ide driver in favor of the pata one
pata/at91: use newly introduced SMC accessors
ARM: at91: add accessor to manage SMC
ARM: at91:rtc/rtc-at91sam9: ioremap register bank
ARM: at91: USB AT91 gadget registration for module
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Driver at91_ide is broken and should not be fixed: remove it.
Modification of device files that where making use of it. The
PATA driver (pata_at91) is able to replace at91_ide.
Signed-off-by: Jean-Christophe PLAGNIOL-VILLARD <plagnioj@jcrosoft.com>
Acked-by: Nicolas Ferre <nicolas.ferre@atmel.com>
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SMC, Static Memory Controller will need more accessors to fine
configure its parameters.
Signed-off-by: Jean-Christophe PLAGNIOL-VILLARD <plagnioj@jcrosoft.com>
Acked-by: Nicolas Ferre <nicolas.ferre@atmel.com>
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Registration of at91_udc as a module will enable SoC
related code.
Fix following an idea from Karel Znamenacek.
Signed-off-by: Nicolas Ferre <nicolas.ferre@atmel.com>
Acked-by: Karel Znamenacek <karel@ryston.cz>
Acked-by: Jean-Christophe PLAGNIOL-VILLARD <plagnioj@jcrosoft.com>
Cc: stable <stable@vger.kernel.org>
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git://git.kernel.org/pub/scm/linux/kernel/git/tmlind/linux-omap into fixes
* 'fixes' of git://git.kernel.org/pub/scm/linux/kernel/git/tmlind/linux-omap:
ARM: OMAP2xxx: PM: fix OMAP2xxx-specific UART idle bug in v3.3
ARM: OMAP3: cm-t35: fix section mismatch warning
ARM: OMAP2: Fix the OMAP2 only build break seen with 2011+ ARM tool-chains
ARM: OMAP2+: board-generic: Add missing handle_irq callbacks
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On OMAP2420-based systems, the PM code ignores the state of the UART
functional clocks when determining what idle state to enter. This
breaks the serial port now that the UART driver's clock behavior can
be controlled via the PM autosuspend timeout.
To fix, remove the special-case idle handling for the UARTs in the
OMAP2420/2430 PM idle code added by commit
4af4016c53f52b26461b8030211f8427a58fa5ed ("OMAP3: PM: UART: disable
clocks when idle and off-mode support").
Tested on Nokia N800. This patch is a collaboration between Tony
Lindgren <tony@atomide.com> and Paul Walmsley <paul@pwsan.com>.
Signed-off-by: Paul Walmsley <paul@pwsan.com>
Acked-by: Kevin Hilman <khilman@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
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WARNING: arch/arm/mach-omap2/built-in.o(.text+0xeae8):
Section mismatch in reference from the function cm_t35_init_usbh()
to the (unknown reference) .init.data:(unknown)
The function cm_t35_init_usbh() references
the (unknown reference) __initdata (unknown).
This is often because cm_t35_init_usbh lacks a __initdata
annotation or the annotation of (unknown) is wrong.
Signed-off-by: Igor Grinberg <grinberg@compulab.co.il>
Signed-off-by: Tony Lindgren <tony@atomide.com>
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With the latest Sourcery G++ Lite 2011.03-41 and latest linaro
tool-chains OMAP2 only build breaks with below error.
arch/arm/mach-omap2/omap-smc.S: Assembler messages:
arch/arm/mach-omap2/omap-smc.S:30: Error: selected processor does not support ARM mode `smc #0'
arch/arm/mach-omap2/omap-smc.S:53: Error: selected processor does not support ARM mode `smc #0'
arch/arm/mach-omap2/omap-smc.S:61: Error: selected processor does not support ARM mode `smc #0'
arch/arm/mach-omap2/omap-smc.S:69: Error: selected processor does not support ARM mode `smc #0'
arch/arm/mach-omap2/omap-smc.S:77: Error: selected processor does not support ARM mode `smc #0'
make[1]: *** [arch/arm/mach-omap2/omap-smc.o] Error 1
OMAP2 devices doesn't have the security support but the security support
was getting built because of OMAP2PLUS. Don't build security code for
OMAP2 devices.
While at it, fix the secure-common line in the Makefile to use tabs
instead of spaces.
Reported-by: Kevin Hilman <khilman@ti.com>
Signed-off-by: Santosh Shilimkar <santosh.shilimkar@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
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The following commit: 6b2f55d7851aa358d3a99cff344c560c4967f042,
is adding the support for the CONFIG_MULTI_IRQ_HANDLER but did
not update all the machine descriptors supported in the DT
board-generic.c file.
It thus break the DT boot on OMAP3 and OMAP4 boards.
Add the proper handle_irq callbacks for OMAP3 and OMAP4 generic
machine descriptors.
Signed-off-by: Benoit Cousson <b-cousson@ti.com>
Acked-by: Marc Zyngier <marc.zyngier@arm.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
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Fix build breakage due to the following commits:
Commit bd5f12a24766c1f299def0a78b008d4746f528f2
ARM: 7042/3: mach-ep93xx: break out GPIO driver specifics
Commit 257af9f9725aa8a863b306659208a031135d59e7
ARM: 7041/1: gpio-ep93xx: hookup the to_irq callback in the driver
The vision_ep9307 machine uses the ep93xx build-in gpios and needs to
include <mach/gpio-ep93xx.h> to pickup the defines.
The gpio_to_irq() call is now a callback to the gpio-ep93xx.c driver
and cannot be used as a constant initializer for the .irq member of
struct i2c_board_info.
Signed-off-by: Hartley Sweeten <hsweeten@visionengravers.com>
Acked-by: Ryan Mallon <rmallon@gmail.com>
Acked-by: Mika Westerberg <mika.westerberg@iki.fi>
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
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git://git.kernel.org/pub/scm/linux/kernel/git/kgene/linux-samsung into fixes
* 'v3.3-samsung-fixes-3' of git://git.kernel.org/pub/scm/linux/kernel/git/kgene/linux-samsung: (2 commits)
ARM: EXYNOS: Add cpu-offset property in gic device tree node
ARM: EXYNOS: Bring exynos4-dt up to date
Linux 3.3-rc3
This includes an update to the v3.3-rc3 release from v3.3-rc2
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
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Commit db0d4db22a78 ('ARM: gic: allow GIC to support non-banked setups)
requires a cpu-offset property to be specified for non-banked gic
controllers, which is the case for Exynos4.
Reported-and-Tested-by: Karol Lewandowski <k.lewandowsk@samsung.com>
Signed-off-by: Thomas Abraham <thomas.abraham@linaro.org>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
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This commit brings exynos4-dt in line with recent changes to
mach-exynos tree, specifically:
- Fixes build break related to replacing plat/exynos4.h with
common.h in commit cc511b8d84d8 ("ARM: 7257/1: EXYNOS:
introduce arch/arm/mach-exynos/common.[ch]")
- Converts machine to use CONFIG_MULTI_IRQ_HANDLER as done for
other machines in commit 4e44d2cb95bd ("ARM: exynos4: convert
to CONFIG_MULTI_IRQ_HANDLER")
- Adds restart specifier as done for other machines in commit
9eb4859564d6 ("ARM: 7262/1: restart: EXYNOS: use new restart hook")
Signed-off-by: Karol Lewandowski <k.lewandowsk@samsung.com>
Signed-off-by: Kyungmin Park <kyungmin.park@samsung.com>
Cc: Thomas Abraham <thomas.abraham@linaro.org>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
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git://git.kernel.org/pub/scm/linux/kernel/git/olof/tegra into fixes
* 'fixes' of git://git.kernel.org/pub/scm/linux/kernel/git/olof/tegra:
ARM: tegra: paz00: fix wrong UART port on mini-pcie plug
ARM: tegra: paz00: fix wrong SD1 power gpio
i2c: tegra: Add devexit_p() for remove
ARM: tegra: dma: fix buildbreak for !CONFIG_TEGRA_SYSTEM_DMA
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UARTC is connected to the mini-pcie port.
Signed-off-by: Marc Dietrich <marvin24@gmx.de>
Acked-by: Stephen Warren <swarren@nvidia.com>
Signed-off-by: Olof Johansson <olof@lixom.net>
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The power gpio for the external memory card was specified wrongly.
Replace it with the correct value (tested with warmboot with fastboot).
Signed-off-by: Marc Dietrich <marvin24@gmx.de>
Acked-by: Stephen Warren <swarren@nvidia.com>
Signed-off-by: Olof Johansson <olof@lixom.net>
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There's no need to keep the DMA_REQ_SEL defines inside the ifdef.
Fixes the following build break with CONFIG_TEGRA_SYSTEM_DMA=n:
arch/arm/mach-tegra/devices.c:645: error: 'TEGRA_DMA_REQ_SEL_I2S_1' undeclared here (not in a function)
arch/arm/mach-tegra/devices.c:663: error: 'TEGRA_DMA_REQ_SEL_I2S2_1' undeclared here (not in a function)
arch/arm/mach-tegra/devices.c:663: error: initializer element is not constant
arch/arm/mach-tegra/devices.c:663: error: (near initialization for 'i2s_resource2[1].start')
arch/arm/mach-tegra/devices.c:664: error: initializer element is not constant
arch/arm/mach-tegra/devices.c:664: error: (near initialization for 'i2s_resource2[1].end')
Signed-off-by: Olof Johansson <olof@lixom.net>
Acked-by: Stephen Warren <swarren@nvidia.com>
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The patch "ARM: orion: Consolidate USB platform setup code.", commit
4fcd3f374a928081d391cd9a570afe3b2c692fdc broke USB on TS-7800 and
other orion5x boards, because the wrong type of PHY was being passed
to the EHCI driver in the platform data. Orion5x needs EHCI_PHY_ORION
and all the others want EHCI_PHY_NA.
Allow the mach- code to tell the generic plat-orion code which USB PHY
enum to place into the platform data.
Version 2: Rebase to v3.3-rc2.
Reported-by: Ambroz Bizjak <ambrop7@gmail.com>
Signed-off-by: Andrew Lunn <andrew@lunn.ch>
Tested-by: Ambroz Bizjak <ambrop7@gmail.com>
Acked-by: Nicolas Pitre <nico@linaro.org>
Signed-off-by: Olof Johansson <olof@lixom.net>
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Patchset "ARM: orion: Refactor the MPP code common in the orion
platform" broke at least Orion5x based platforms. These platforms have
pins configured as GPIO when the selector is not 0x0. However the
common code assumes the selector is always 0x0 for a GPIO lines. It
then ignores the GPIO bits in the MPP definitions, resulting in that
Orion5x machines cannot correctly configure there GPIO lines.
The Fix removes the assumption that the selector is always 0x0.
In order that none GPIO configurations are correctly blocked,
Kirkwood and mv78xx0 MPP definitions are corrected to only set the
GPIO bits for GPIO configurations.
This third version, which does not contain any whitespace changes,
and is rebased on v3.3-rc2.
Signed-off-by: Andrew Lunn <andrew@lunn.ch>
Acked-by: Nicolas Pitre <nico@linaro.org>
Signed-off-by: Olof Johansson <olof@lixom.net>
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git://git.kernel.org/pub/scm/linux/kernel/git/kgene/linux-samsung into fixes
* 'v3.3-samsung-fixes-2' of git://git.kernel.org/pub/scm/linux/kernel/git/kgene/linux-samsung:
ARM: EXYNOS: Correct M-5MOLS sensor clock frequency on Universal C210 board
ARM: EXYNOS: Correct framebuffer window size on Nuri board
ARM: SAMSUNG: Fix missing api-change from subsys_interface change
ARM: EXYNOS: Fix "warning: initialization from incompatible pointer type"
ARM: S5PV210: Fix the name of exynos4_clk_hdmiphy_ctrl() for S5PV210
ARM: EXYNOS: Remove build warning without enabling PM
ARM: SAMSUNG: Fix platform data setup for I2C adapter 0
ARM: EXYNOS: fix non-SMP builds for EXYNOS4
ARM: S3C6410: Use device names for both I2C clocks
ARM: S3C64XX: Make s3c64xx_init_uarts() static
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In order to keep the sensor's master clock frequency in valid range
when FIMC parent clock is xusbxti, the specified frequency must be
exactly 24MHZ, otherwise it's being set to too low value due to
rounding.
Signed-off-by: Sylwester Nawrocki <s.nawrocki@samsung.com>
Signed-off-by: Kyungmin Park <kyungmin.park@samsung.com>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
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The real LCD resolution on Nuri is 1024x600, not 1280x800. This change
fixes the color distortion (green shadows) on half of the screen.
Also increase framebuffer virtual size for display panning support.
Signed-off-by: Sylwester Nawrocki <s.nawrocki@samsung.com>
Signed-off-by: Marek Szyprowski <m.szyprowski@samsung.com>
Signed-off-by: Kyungmin Park <kyungmin.park@samsung.com>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
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Commit 4a858cfc9a (arm: convert sysdev_class to a regular subsystem)
converted the samsung sysdevs into subsys_interface instances.
While the original add-function only had a (struct sys_device *)
parameter, the dev_add from subsys_interface needs
(struct device *, struct subsys_interface *)
leading to "initialized from incompatible pointer type" warnings.
Signed-off-by: Heiko Stuebner <heiko@sntech.de>
Cc: Greg Kroah-Hartman <gregkh@suse.de>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
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Fix the wrong function prototype.
Signed-off-by: Jonghwan Choi <jhbird.choi@samsung.com>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
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Should be s5pv210_clk_hdmiphy_ctrl() in mach-s5pv210/.
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
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Fixed following build warning with exynos4_defconfig.
arch/arm/mach-exynos/clock.c:33: warning: 'exynos4_clock_save' defined but not used
arch/arm/mach-exynos/clock-exynos4210.c:35: warning: 'exynos4210_clock_save' defined but not used
arch/arm/mach-exynos/clock-exynos4212.c:35: warning: 'exynos4212_clock_save' defined but not used
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
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The common static default_i2c_data structure gets bus_num set by each
s3c_i2c?_set_platdata() call, except for s3c_i2c0_set_platdata(). Thus
if for instance s3c_i2c1_set_platdata() is called prior to
s3c_i2c0_set_platdata() the I2C0 controller has bus_num set to wrong value
of 1, i.e. the one from previous set_platdata call. Fix this by also setting
bus_num for I2C0.
Signed-off-by: Sylwester Nawrocki <s.nawrocki@samsung.com>
Signed-off-by: Kyungmin Park <kyungmin.park@samsung.com>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
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This patch fixes the following build issue, which happens only if
SMP has been disabled:
arch/arm/mach-exynos/built-in.o: In function `exynos4_pm_resume':
arch/arm/mach-exynos/pm.c:387: undefined reference to `scu_enable'
Signed-off-by: Marek Szyprowski <m.szyprowski@samsung.com>
Signed-off-by: Kyungmin Park <kyungmin.park@samsung.com>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
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When the S3C64xx CPUs were converted to clkdev mappings were added for the
I2C controllers on them. On S3C6410 a device name is specified for I2C
controller 1 but not for controller 0 which makes the code less robust as
we'll falsely return the clock for controller 0 if there's an error in the
request for controller 1.
Improve things by registering a device name for controller 0 as well. Due
to the fact that we change the numbering for controller 0 depending on if
we've registered controller 1 this requires an ifdef to choose the name.
Signed-off-by: Mark Brown <broonie@opensource.wolfsonmicro.com>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
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Now that it's in common.c it's not used in multiple source files.
Signed-off-by: Mark Brown <broonie@opensource.wolfsonmicro.com>
Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>
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git://git.kernel.org/pub/scm/linux/kernel/git/benh/powerpc
Here are a few more fixes for powerpc. Some are regressions, the rest
is simple/obvious/nasty enough that I deemed it good to go now.
Here's also step one of deprecating legacy iSeries support: we are
removing it from the main defconfig.
Nobody seems to be using it anymore and the code is nasty to maintain,
(involves horrible hacks in various low level areas of the kernel) so we
plan to actually rip it out at some point. For now let's just avoid
building it by default. Stephen will proceed to do the actual removal
later (probably 3.4 or 3.5).
* 'merge' of git://git.kernel.org/pub/scm/linux/kernel/git/benh/powerpc:
powerpc/perf: power_pmu_start restores incorrect values, breaking frequency events
powerpc/adb: Use set_current_state()
powerpc: Disable interrupts early in Program Check
powerpc: Remove legacy iSeries from ppc64_defconfig
powerpc/fsl/pci: Fix PCIe fixup regression
powerpc: Fix kernel log of oops/panic instruction dump
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events
perf on POWER stopped working after commit e050e3f0a71b (perf: Fix
broken interrupt rate throttling). That patch exposed a bug in
the POWER perf_events code.
Since the PMCs count upwards and take an exception when the top bit
is set, we want to write 0x80000000 - left in power_pmu_start. We were
instead programming in left which effectively disables the counter
until we eventually hit 0x80000000. This could take seconds or longer.
With the patch applied I get the expected number of samples:
SAMPLE events: 9948
Signed-off-by: Anton Blanchard <anton@samba.org>
Acked-by: Paul Mackerras <paulus@samba.org>
Signed-off-by: Benjamin Herrenschmidt <benh@kernel.crashing.org>
Cc: <stable@kernel.org>
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Program Check exceptions are the result of WARNs, BUGs, some
type of breakpoints, kprobe, and other illegal instructions.
We want interrupts (and thus preemption) to remain disabled
while doing the initial stage of testing the reason and
branching off to a debugger or kprobe, so we are still on
the original CPU which makes debugging easier in various cases.
This is how the code was intended, hence the local_irq_enable()
right in the middle of program_check_exception().
However, the assembly exception prologue for that exception was
incorrectly marked as enabling interrupts, which defeats that
(and records a redundant enable with lockdep).
Signed-off-by: Benjamin Herrenschmidt <benh@kernel.crashing.org>
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Since we are heading towards removing the Legacy iSeries platform, start
by no longer building it for ppc64_defconfig.
Signed-off-by: Stephen Rothwell <sfr@canb.auug.org.au>
Signed-off-by: Benjamin Herrenschmidt <benh@kernel.crashing.org>
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