| Commit message (Collapse) | Author | Age | Files | Lines |
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git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty
Pull tty/serial driver fixes from Greg KH:
"Here are some small tty and serial driver fixes for 6.2-rc5 that
resolve a number of tiny reported issues and some new device ids. They
include:
- new device id for the exar serial driver
- speakup tty driver bugfix
- atmel serial driver baudrate fixup
- stm32 serial driver bugfix and then revert as the bugfix broke the
build. That will come back in a later pull request once it is all
worked out properly.
- amba-pl011 serial driver rs486 mode bugfix
- qcom_geni serial driver bugfix
Most of these have been in linux-next with no reported problems (well,
other than the build breakage which generated the revert), the new
device id passed 0-day testing"
* tag 'tty-6.2-rc5' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty:
serial: exar: Add support for Sealevel 7xxxC serial cards
Revert "serial: stm32: Merge hard IRQ and threaded IRQ handling into single IRQ handler"
tty: serial: qcom_geni: avoid duplicate struct member init
serial: atmel: fix incorrect baudrate setup
tty: fix possible null-ptr-defer in spk_ttyio_release
serial: stm32: Merge hard IRQ and threaded IRQ handling into single IRQ handler
serial: amba-pl011: fix high priority character transmission in rs486 mode
serial: pch_uart: Pass correct sg to dma_unmap_sg()
tty: serial: qcom-geni-serial: fix slab-out-of-bounds on RX FIFO buffer
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Add support for Sealevel 7xxxC serial cards.
This patch:
* Adds IDs to recognize 7xxxC cards from Sealevel Systems.
* Updates exar_pci_probe() to set nr_ports to last two bytes of primary
dev ID for these cards.
Signed-off-by: Matthew Howell <matthew.howell@sealevel.com>
Cc: stable <stable@kernel.org>
Link: https://lore.kernel.org/r/alpine.DEB.2.21.2301191440010.22558@tstest-VirtualBox
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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IRQ handler"
This reverts commit f24771b62a83239f0dce816bddf0f6807f436235 as it is
reported to break the build.
Reported-by: kernel test robot <lkp@intel.com>
Link: https://lore.kernel.org/r/202301200130.ttBiTzfO-lkp@intel.com
Fixes: f24771b62a83 ("serial: stm32: Merge hard IRQ and threaded IRQ handling into single IRQ handler")
Cc: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Cc: Valentin Caron <valentin.caron@foss.st.com> # V3
Cc: Marek Vasut <marex@denx.de>
Cc: Johan Hovold <johan@kernel.org>
Cc: stable@vger.kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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When -Woverride-init is enabled in a build, gcc points out that
qcom_geni_serial_pm_ops contains conflicting initializers:
drivers/tty/serial/qcom_geni_serial.c:1586:20: error: initialized field overwritten [-Werror=override-init]
1586 | .restore = qcom_geni_serial_sys_hib_resume,
| ^~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~
drivers/tty/serial/qcom_geni_serial.c:1586:20: note: (near initialization for 'qcom_geni_serial_pm_ops.restore')
drivers/tty/serial/qcom_geni_serial.c:1587:17: error: initialized field overwritten [-Werror=override-init]
1587 | .thaw = qcom_geni_serial_sys_hib_resume,
| ^~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~
Open-code the initializers with the version that was already used,
and use the pm_sleep_ptr() method to deal with unused ones,
in place of the __maybe_unused annotation.
Fixes: 35781d8356a2 ("tty: serial: qcom-geni-serial: Add support for Hibernation feature")
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
Reviewed-by: Douglas Anderson <dianders@chromium.org>
Link: https://lore.kernel.org/r/20221215165453.1864836-1-arnd@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Commit ba47f97a18f2 ("serial: core: remove baud_rates when serial console
setup") changed uart_set_options to select the correct baudrate
configuration based on the absolute error between requested baudrate and
available standard baudrate settings.
Prior to that commit the baudrate was selected based on which predefined
standard baudrate did not exceed the requested baudrate.
This change of selection logic was never reflected in the atmel serial
driver. Thus the comment left in the atmel serial driver is no longer
accurate.
Additionally the manual rounding up described in that comment and applied
via (quot - 1) requests an incorrect baudrate. Since uart_set_options uses
tty_termios_encode_baud_rate to determine the appropriate baudrate flags
this can cause baudrate selection to fail entirely because
tty_termios_encode_baud_rate will only select a baudrate if relative error
between requested and selected baudrate does not exceed +/-2%.
Fix that by requesting actual, exact baudrate used by the serial.
Fixes: ba47f97a18f2 ("serial: core: remove baud_rates when serial console setup")
Cc: stable <stable@kernel.org>
Signed-off-by: Tobias Schramm <t.schramm@manjaro.org>
Acked-by: Richard Genoud <richard.genoud@gmail.com>
Link: https://lore.kernel.org/r/20230109072940.202936-1-t.schramm@manjaro.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Requesting an interrupt with IRQF_ONESHOT will run the primary handler
in the hard-IRQ context even in the force-threaded mode. The
force-threaded mode is used by PREEMPT_RT in order to avoid acquiring
sleeping locks (spinlock_t) in hard-IRQ context. This combination
makes it impossible and leads to "sleeping while atomic" warnings.
Use one interrupt handler for both handlers (primary and secondary)
and drop the IRQF_ONESHOT flag which is not needed.
Fixes: e359b4411c283 ("serial: stm32: fix threaded interrupt handling")
Reviewed-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Tested-by: Valentin Caron <valentin.caron@foss.st.com> # V3
Signed-off-by: Marek Vasut <marex@denx.de>
Cc: stable@vger.kernel.org
Link: https://lore.kernel.org/r/20230112180417.25595-1-marex@denx.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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In RS485 mode the transmission of a high priority character fails since it
is written to the data register before the transmitter is enabled. Fix this
in pl011_tx_chars() by enabling RS485 transmission before writing the
character.
Fixes: 8d479237727c ("serial: amba-pl011: add RS485 support")
Cc: stable@vger.kernel.org
Signed-off-by: Lino Sanfilippo <l.sanfilippo@kunbus.com>
Link: https://lore.kernel.org/r/20230108181735.10937-1-LinoSanfilippo@gmx.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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A local variable sg is used to store scatterlist pointer in
pch_dma_tx_complete(). The for loop doing Tx byte accounting before
dma_unmap_sg() alters sg in its increment statement. Therefore, the
pointer passed into dma_unmap_sg() won't match to the one given to
dma_map_sg().
To fix the problem, use priv->sg_tx_p directly in dma_unmap_sg()
instead of the local variable.
Fixes: da3564ee027e ("pch_uart: add multi-scatter processing")
Cc: stable@vger.kernel.org
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20230103093435.4396-1-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Driver's probe allocates memory for RX FIFO (port->rx_fifo) based on
default RX FIFO depth, e.g. 16. Later during serial startup the
qcom_geni_serial_port_setup() updates the RX FIFO depth
(port->rx_fifo_depth) to match real device capabilities, e.g. to 32.
The RX UART handle code will read "port->rx_fifo_depth" number of words
into "port->rx_fifo" buffer, thus exceeding the bounds. This can be
observed in certain configurations with Qualcomm Bluetooth HCI UART
device and KASAN:
Bluetooth: hci0: QCA Product ID :0x00000010
Bluetooth: hci0: QCA SOC Version :0x400a0200
Bluetooth: hci0: QCA ROM Version :0x00000200
Bluetooth: hci0: QCA Patch Version:0x00000d2b
Bluetooth: hci0: QCA controller version 0x02000200
Bluetooth: hci0: QCA Downloading qca/htbtfw20.tlv
bluetooth hci0: Direct firmware load for qca/htbtfw20.tlv failed with error -2
Bluetooth: hci0: QCA Failed to request file: qca/htbtfw20.tlv (-2)
Bluetooth: hci0: QCA Failed to download patch (-2)
==================================================================
BUG: KASAN: slab-out-of-bounds in handle_rx_uart+0xa8/0x18c
Write of size 4 at addr ffff279347d578c0 by task swapper/0/0
CPU: 0 PID: 0 Comm: swapper/0 Not tainted 6.1.0-rt5-00350-gb2450b7e00be-dirty #26
Hardware name: Qualcomm Technologies, Inc. Robotics RB5 (DT)
Call trace:
dump_backtrace.part.0+0xe0/0xf0
show_stack+0x18/0x40
dump_stack_lvl+0x8c/0xb8
print_report+0x188/0x488
kasan_report+0xb4/0x100
__asan_store4+0x80/0xa4
handle_rx_uart+0xa8/0x18c
qcom_geni_serial_handle_rx+0x84/0x9c
qcom_geni_serial_isr+0x24c/0x760
__handle_irq_event_percpu+0x108/0x500
handle_irq_event+0x6c/0x110
handle_fasteoi_irq+0x138/0x2cc
generic_handle_domain_irq+0x48/0x64
If the RX FIFO depth changes after probe, be sure to resize the buffer.
Fixes: f9d690b6ece7 ("tty: serial: qcom_geni_serial: Allocate port->rx_fifo buffer in probe")
Cc: <stable@vger.kernel.org>
Signed-off-by: Krzysztof Kozlowski <krzysztof.kozlowski@linaro.org>
Reviewed-by: Jiri Slaby <jirislaby@kernel.org>
Link: https://lore.kernel.org/r/20221221164022.1087814-1-krzysztof.kozlowski@linaro.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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git://git.kernel.org/pub/scm/linux/kernel/git/printk/linux
Pull printk fixes from Petr Mladek:
- Prevent a potential deadlock when configuring kgdb console
- Fix a kernel doc warning
* tag 'printk-for-6.2-rc5' of git://git.kernel.org/pub/scm/linux/kernel/git/printk/linux:
kernel/printk/printk.c: Fix W=1 kernel-doc warning
tty: serial: kgdboc: fix mutex locking order for configure_kgdboc()
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Several mutexes are taken while setting up console serial ports. In
particular, the tty_port->mutex and @console_mutex are taken:
serial_pnp_probe
serial8250_register_8250_port
uart_add_one_port (locks tty_port->mutex)
uart_configure_port
register_console (locks @console_mutex)
In order to synchronize kgdb's tty_find_polling_driver() with
register_console(), commit 6193bc90849a ("tty: serial: kgdboc:
synchronize tty_find_polling_driver() and register_console()") takes
the @console_mutex. However, this leads to the following call chain
(with locking):
platform_probe
kgdboc_probe
configure_kgdboc (locks @console_mutex)
tty_find_polling_driver
uart_poll_init (locks tty_port->mutex)
uart_set_options
This is clearly deadlock potential due to the reverse lock ordering.
Since uart_set_options() requires holding @console_mutex in order to
serialize early initialization of the serial-console lock, take the
@console_mutex in uart_poll_init() instead of configure_kgdboc().
Since configure_kgdboc() was using @console_mutex for safe traversal
of the console list, change it to use the SRCU iterator instead.
Add comments to uart_set_options() kerneldoc mentioning that it
requires holding @console_mutex (aka the console_list_lock).
Fixes: 6193bc90849a ("tty: serial: kgdboc: synchronize tty_find_polling_driver() and register_console()")
Signed-off-by: John Ogness <john.ogness@linutronix.de>
Reviewed-by: Sergey Senozhatsky <senozhatsky@chromium.org>
Reviewed-by: Petr Mladek <pmladek@suse.com>
[pmladek@suse.com: Export console_srcu_read_lock_is_held() to fix build kgdboc as a module.]
Signed-off-by: Petr Mladek <pmladek@suse.com>
Link: https://lore.kernel.org/r/20230112161213.1434854-1-john.ogness@linutronix.de
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git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty
Pull tty/serial driver updates from Greg KH:
"Here is the "big" set of tty/serial driver changes for 6.2-rc1.
As in previous kernel releases, nothing big here at all, just some
small incremental serial/tty layer cleanups and some individual driver
additions and fixes. Highlights are:
- serial helper macros from Jiri Slaby to reduce the amount of
duplicated code in serial drivers
- api cleanups and consolidations from Ilpo Järvinen in lots of
serial drivers
- the usual set of n_gsm fixes from Daniel Starke as that code gets
exercised more
- TIOCSTI is finally able to be disabled if requested (security
hardening feature from Kees Cook)
- fsl_lpuart driver fixes and features added
- other small serial driver additions and fixes
All of these have been in linux-next for a while with no reported
problems"
* tag 'tty-6.2-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty: (97 commits)
serial: atmel: don't stop the transmitter when doing PIO
serial: atmel: cleanup atmel_start+stop_tx()
tty: serial: fsl_lpuart: switch to new dmaengine_terminate_* API
serial: sunsab: Fix error handling in sunsab_init()
serial: altera_uart: fix locking in polling mode
serial: pch: Fix PCI device refcount leak in pch_request_dma()
tty: serial: fsl_lpuart: Use pm_ptr() to avoid need to make pm __maybe_unused
tty: serial: fsl_lpuart: Add runtime pm support
tty: serial: fsl_lpuart: enable wakeup source for lpuart
serdev: Replace poll loop by readx_poll_timeout() macro
tty: synclink_gt: unwind actions in error path of net device open
serial: stm32: move dma_request_chan() before clk_prepare_enable()
dt-bindings: serial: xlnx,opb-uartlite: Drop 'contains' from 'xlnx,use-parity'
serial: pl011: Do not clear RX FIFO & RX interrupt in unthrottle.
serial: amba-pl011: avoid SBSA UART accessing DMACR register
tty: serial: altera_jtaguart: remove struct altera_jtaguart
tty: serial: altera_jtaguart: use uart_port::read_status_mask
tty: serial: altera_jtaguart: remove unused altera_jtaguart::sigs
tty: serial: altera_jtaguart: remove flag from altera_jtaguart_rx_chars()
n_tty: Rename tail to old_tail in n_tty_read()
...
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Writing ATMEL_US_TXDIS to ATMEL_US_CR makes the transmitter NOT to send
the just queued character. This means when the character is last and
uart calls ops->stop_tx(), the character is not sent at all.
The usart datasheet is not much specific on this, it just says the
transmitter is stopped. But apparently, the character is dropped. So
we should stop the transmitter only for DMA and PDC transfers to not
send any more characters. For PIO, this is unexpected and deviates from
other drivers. In particular, the below referenced commit broke TX as it
added a call to ->stop_tx() after the very last character written to the
transmitter.
So fix this by limiting the write of ATMEL_US_TXDIS to DMA transfers
only.
Even there, I don't know if it is correctly implemented. Are all the
queued characters sent once ->start_tx() is called? Anyone tested flow
control -- be it hard (RTSCTS) or the soft (XOFF/XON) one?
Fixes: 2d141e683e9a ("tty: serial: use uart_port_tx() helper")
Cc: Richard Genoud <richard.genoud@gmail.com>
Cc: Nicolas Ferre <nicolas.ferre@microchip.com>
Cc: Alexandre Belloni <alexandre.belloni@bootlin.com>
Cc: Claudiu Beznea <claudiu.beznea@microchip.com>
Cc: linux-arm-kernel@lists.infradead.org
Reported-by: Michael Walle <michael@walle.cc>
Signed-off-by: Jiri Slaby (SUSE) <jirislaby@kernel.org>
Link: https://lore.kernel.org/r/20221123082736.24566-2-jirislaby@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Define local variables holding information about whether pdc or dma is
used in the HW. These are retested several times by calls to
atmel_use_pdc_tx() and atmel_use_dma_tx(). So to make the code more
readable, simply cache the values.
This is also a preparatory patch for the next one (where is_pdc is used
once more in atmel_stop_tx()).
Cc: Richard Genoud <richard.genoud@gmail.com>
Cc: Nicolas Ferre <nicolas.ferre@microchip.com>
Cc: Alexandre Belloni <alexandre.belloni@bootlin.com>
Cc: Claudiu Beznea <claudiu.beznea@microchip.com>
Cc: linux-arm-kernel@lists.infradead.org
Reported-by: Michael Walle <michael@walle.cc>
Signed-off-by: Jiri Slaby (SUSE) <jirislaby@kernel.org>
Link: https://lore.kernel.org/r/20221123082736.24566-1-jirislaby@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Convert dmaengine_terminate_all() calls to synchronous and asynchronous
versions where appropriate.
Signed-off-by: Sherry Sun <sherry.sun@nxp.com>
Link: https://lore.kernel.org/r/20221123023619.30173-1-sherry.sun@nxp.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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The sunsab_init() returns the platform_driver_register() directly without
checking its return value, if platform_driver_register() failed, the
allocated sunsab_ports is leaked.
Fix by free sunsab_ports and set it to NULL when platform_driver_register()
failed.
Fixes: c4d37215a824 ("[SERIAL] sunsab: Convert to of_driver framework.")
Signed-off-by: Yuan Can <yuancan@huawei.com>
Link: https://lore.kernel.org/r/20221123061212.52593-1-yuancan@huawei.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Since altera_uart_interrupt() may also be called from
a poll timer in "serving_softirq" context, use
spin_[lock_irqsave|unlock_irqrestore] variants, which
are appropriate for both softirq and hardware interrupt
contexts.
Fixes: 2f8b9c15cd88 ("altera_uart: Add support for polling mode (IRQ-less)")
Signed-off-by: Gabriel Somlo <gsomlo@gmail.com>
Link: https://lore.kernel.org/r/20221122200426.888349-1-gsomlo@gmail.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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As comment of pci_get_slot() says, it returns a pci_device with its
refcount increased. The caller must decrement the reference count by
calling pci_dev_put().
Since 'dma_dev' is only used to filter the channel in filter(), we can
call pci_dev_put() before exiting from pch_request_dma(). Add the
missing pci_dev_put() for the normal and error path.
Fixes: 3c6a483275f4 ("Serial: EG20T: add PCH_UART driver")
Signed-off-by: Xiongfeng Wang <wangxiongfeng2@huawei.com>
Link: https://lore.kernel.org/r/20221122114559.27692-1-wangxiongfeng2@huawei.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Use pm_ptr() to remove the need to mark the pm functions as
__maybe_unused when the kernel is built without CONFIG_PM support.
Signed-off-by: Sherry Sun <sherry.sun@nxp.com>
Link: https://lore.kernel.org/r/20221110113859.8485-4-sherry.sun@nxp.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Add runtime pm support to manage the lpuart clock.
Signed-off-by: Sherry Sun <sherry.sun@nxp.com>
Link: https://lore.kernel.org/r/20221110113859.8485-3-sherry.sun@nxp.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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LPUART supports both synchronous wakeup and asynchronous wakeup(wakeup
the system when the UART clocks are shut-off), the synchronous wakeup is
configured by UARTCTRL_RIE interrupt, and the asynchronous wakeup is
configured by UARTBAUD_RXEDGIE interrupt.
Add lpuart_uport_is_active() to determine if the uart port needs to get
into the suspend states, also add lpuart_suspend_noirq() and
lpuart_resume_noirq() to enable and disable the wakeup irq bits if the
uart port needs to be set as wakeup source.
When use lpuart with DMA mode, it still needs to switch to the cpu mode
in .suspend() that enable cpu interrupts RIE and RXEDGIE as wakeup
source, after system resume back, needs to setup DMA again, .resume()
will share the HW setup code with .startup(), so abstract the same code
to the api like lpuart32_hw_setup().
Signed-off-by: Sherry Sun <sherry.sun@nxp.com>
Link: https://lore.kernel.org/r/20221110113859.8485-2-sherry.sun@nxp.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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If dma_request_chan() returns a PROBE_DEFER error, clk_disable_unprepare()
will be called and USART clock will be disabled. But early console can be
still active on the same USART.
While moving dma_request_chan() before clk_prepare_enable(), the clock
won't be taken in case of a DMA PROBE_DEFER error, and so it doesn't need
to be disabled. Then USART is still clocked for early console.
Fixes: a7770a4bfcf4 ("serial: stm32: defer probe for dma devices")
Reported-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Valentin Caron <valentin.caron@foss.st.com>
Link: https://lore.kernel.org/r/20221118170602.1057863-1-valentin.caron@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Clearing the RX FIFO will cause data loss.
Copy the pl011_enabl_interrupts implementation, and remove the clear
interrupt and FIFO part of the code.
Fixes: 211565b10099 ("serial: pl011: UPSTAT_AUTORTS requires .throttle/unthrottle")
Signed-off-by: delisun <delisun@pateo.com.cn>
Reviewed-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20221110020108.7700-1-delisun@pateo.com.cn
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Chapter "B Generic UART" in "ARM Server Base System Architecture" [1]
documentation describes a generic UART interface. Such generic UART
does not support DMA. In current code, sbsa_uart_pops and
amba_pl011_pops share the same stop_rx operation, which will invoke
pl011_dma_rx_stop, leading to an access of the DMACR register. This
commit adds a using_rx_dma check in pl011_dma_rx_stop to avoid the
access to DMACR register for SBSA UARTs which does not support DMA.
When the kernel enables DMA engine with "CONFIG_DMA_ENGINE=y", Linux
SBSA PL011 driver will access PL011 DMACR register in some functions.
For most real SBSA Pl011 hardware implementations, the DMACR write
behaviour will be ignored. So these DMACR operations will not cause
obvious problems. But for some virtual SBSA PL011 hardware, like Xen
virtual SBSA PL011 (vpl011) device, the behaviour might be different.
Xen vpl011 emulation will inject a data abort to guest, when guest is
accessing an unimplemented UART register. As Xen VPL011 is SBSA
compatible, it will not implement DMACR register. So when Linux SBSA
PL011 driver access DMACR register, it will get an unhandled data abort
fault and the application will get a segmentation fault:
Unhandled fault at 0xffffffc00944d048
Mem abort info:
ESR = 0x96000000
EC = 0x25: DABT (current EL), IL = 32 bits
SET = 0, FnV = 0
EA = 0, S1PTW = 0
FSC = 0x00: ttbr address size fault
Data abort info:
ISV = 0, ISS = 0x00000000
CM = 0, WnR = 0
swapper pgtable: 4k pages, 39-bit VAs, pgdp=0000000020e2e000
[ffffffc00944d048] pgd=100000003ffff803, p4d=100000003ffff803, pud=100000003ffff803, pmd=100000003fffa803, pte=006800009c090f13
Internal error: ttbr address size fault: 96000000 [#1] PREEMPT SMP
...
Call trace:
pl011_stop_rx+0x70/0x80
tty_port_shutdown+0x7c/0xb4
tty_port_close+0x60/0xcc
uart_close+0x34/0x8c
tty_release+0x144/0x4c0
__fput+0x78/0x220
____fput+0x1c/0x30
task_work_run+0x88/0xc0
do_notify_resume+0x8d0/0x123c
el0_svc+0xa8/0xc0
el0t_64_sync_handler+0xa4/0x130
el0t_64_sync+0x1a0/0x1a4
Code: b9000083 b901f001 794038a0 8b000042 (b9000041)
---[ end trace 83dd93df15c3216f ]---
note: bootlogd[132] exited with preempt_count 1
/etc/rcS.d/S07bootlogd: line 47: 132 Segmentation fault start-stop-daemon
This has been discussed in the Xen community, and we think it should fix
this in Linux. See [2] for more information.
[1] https://developer.arm.com/documentation/den0094/c/?lang=en
[2] https://lists.xenproject.org/archives/html/xen-devel/2022-11/msg00543.html
Fixes: 0dd1e247fd39 (drivers: PL011: add support for the ARM SBSA generic UART)
Signed-off-by: Jiamei Xie <jiamei.xie@arm.com>
Reviewed-by: Andre Przywara <andre.przywara@arm.com>
Link: https://lore.kernel.org/r/20221117103237.86856-1-jiamei.xie@arm.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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It contains only struct uart_port, so no need for another structure.
Remove it and convert the rest to use struct uart_port directly.
Cc: Tobias Klauser <tklauser@distanz.ch>
Signed-off-by: Jiri Slaby (SUSE) <jirislaby@kernel.org>
Reviewed-by: Tobias Klauser <tklauser@distanz.ch>
Link: https://lore.kernel.org/r/20221115071724.5185-4-jirislaby@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Instead of self-defined struct altera_jtaguart::imr, use preexisting
uart_port::read_status_mask.
Note that imr was ulong. But there is no reason for that, its values are
uints. And readl/writel's are used to read it/write to it.
Cc: Tobias Klauser <tklauser@distanz.ch>
Signed-off-by: Jiri Slaby (SUSE) <jirislaby@kernel.org>
Reviewed-by: Tobias Klauser <tklauser@distanz.ch>
Link: https://lore.kernel.org/r/20221115071724.5185-3-jirislaby@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Nothing uses struct altera_jtaguart::sigs. Remove it.
Cc: Tobias Klauser <tklauser@distanz.ch>
Signed-off-by: Jiri Slaby (SUSE) <jirislaby@kernel.org>
Reviewed-by: Tobias Klauser <tklauser@distanz.ch>
Link: https://lore.kernel.org/r/20221115071724.5185-2-jirislaby@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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TTY_NORMAL is the only value it contains, so remove the variable and use
the constant instead.
Cc: Tobias Klauser <tklauser@distanz.ch>
Signed-off-by: Jiri Slaby (SUSE) <jirislaby@kernel.org>
Reviewed-by: Tobias Klauser <tklauser@distanz.ch>
Link: https://lore.kernel.org/r/20221115071724.5185-1-jirislaby@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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We need the tty/serial fixes in here as well.
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Commit 801954d1210a ("serial: 8250: 8250_omap: Support native RS485")
calculates RS485 delays from the baudrate. The baudrate is generated
with either a 16x or 13x divisor. The divisor is set in the Mode
Definition Register 1 (MDR1).
The commit erroneously assumes that the register stores the divisor as
a bitmask and uses a logical AND to differentiate between 16x and 13x
divisors. However the divisor is really stored as a 3-bit mode
(see lines 363ff in include/uapi/linux/serial_reg.h).
The logical AND operation is performed with UART_OMAP_MDR1_16X_MODE,
which is defined as 0x0 and hence yields false. So the commit always
assumes a 13x divisor. Fix by using an equal comparison. This works
because we never set any of the other 5 bits in the register. (They
pertain to IrDA mode, which is not supported by the driver).
Fixes: 801954d1210a ("serial: 8250: 8250_omap: Support native RS485")
Link: https://lore.kernel.org/linux-serial/202211070440.8hWunFUN-lkp@intel.com/
Reported-by: kernel test robot <lkp@intel.com>
Reported-by: Dan Carpenter <error27@gmail.com>
Signed-off-by: Lukas Wunner <lukas@wunner.de>
Reviewed-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/7d5b04da13d89b8708b9543a0b125f2b6062a77b.1667977259.git.lukas@wunner.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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A problem about 8250_bcm7271 create debugfs failed is triggered with the
following log given:
[ 324.516635] debugfs: Directory 'bcm7271-uart' with parent '/' already present!
The reason is that brcmuart_init() returns platform_driver_register()
directly without checking its return value, if platform_driver_register()
failed, it returns without destroy the newly created debugfs, resulting
the debugfs of 8250_bcm7271 can never be created later.
brcmuart_init()
debugfs_create_dir() # create debugfs directory
platform_driver_register()
driver_register()
bus_add_driver()
priv = kzalloc(...) # OOM happened
# return without destroy debugfs directory
Fix by removing debugfs when platform_driver_register() returns error.
Fixes: 41a469482de2 ("serial: 8250: Add new 8250-core based Broadcom STB driver")
Signed-off-by: Yuan Can <yuancan@huawei.com>
Link: https://lore.kernel.org/r/20221109072110.117291-2-yuancan@huawei.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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When DMA Rx completes, the current behavior is to just exit the DMA
completion handler without future actions. If the transfer is still
on-going, UART will trigger an interrupt and that eventually rearms the
DMA Rx. The extra interrupt round-trip has an inherent latency cost
that increases the risk of FIFO overrun. In such situations, the
latency margin tends to already be less due to FIFO not being empty.
Add check into DMA Rx completion handler to detect if LSR has DR (Data
Ready) still set. DR indicates there will be more characters pending
and DMA Rx can be rearmed right away to handle them.
Cc: Gilles BULOZ <gilles.buloz@kontron.com>
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Reviewed-by: Andy Shevchenko <andriy.shevchenko@linux.intel.com>
Link: https://lore.kernel.org/r/20221107102126.56481-1-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Fix the two instances of this typo present in the MSM and VT8500 serial
drivers.
Signed-off-by: Jonathan Neuschäfer <j.neuschaefer@gmx.net>
Reviewed-by: Mukesh Ojha <quic_mojha@quicinc.com>
Acked-by: Konrad Dybcio <konrad.dybcio@somainline.org>
Link: https://lore.kernel.org/r/20221104103719.2234098-1-j.neuschaefer@gmx.net
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Use str_enabled_disabled() helper instead of open coding the same.
Reviewed-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Signed-off-by: Andy Shevchenko <andriy.shevchenko@linux.intel.com>
Link: https://lore.kernel.org/r/20221017171633.65275-1-andriy.shevchenko@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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The default polarity of RS485 DE signal is active high. This driver does
not handle such case properly. Currently, when a pin is multiplexed as a
UART CTS_B on boot, this pin is pulled HIGH by the i.MX UART CTS circuit,
which activates DE signal on the RS485 transceiver and thus behave as if
the RS485 was transmitting data, so the system blocks the RS485 bus when
it starts and until user application takes over. This behavior is not OK.
The problem consists of two separate parts.
First, the i.MX UART IP requires UCR1 UARTEN and UCR2 RXEN to be set for
UCR2 CTSC and CTS bits to have any effect. The UCR2 CTSC bit permits the
driver to set CTS (RTS_B or RS485 DE signal) to either level sychronous
to the internal UART IP clock. Compared to other options, like GPIO CTS
control, this has the benefit of being synchronous to the UART IP clock
and thus without glitches or bus delays. The reason for the CTS design
is likely because when the Receiver is disabled, the UART IP can never
indicate that it is ready to receive data by assering CTS signal, so
the CTS is always pulled HIGH by default.
When the port is closed by user space, imx_uart_stop_rx() clears UCR2
RXEN bit, and imx_uart_shutdown() clears UCR1 UARTEN bit. This disables
UART Receiver and UART itself, and forces CTS signal HIGH, which leads
to the RS485 bus being blocked because RS485 DE is incorrectly active.
The proposed solution for this problem is to keep the Receiver running
even after the port is closed, but in loopback mode. This disconnects
the RX FIFO input from the RXD external signal, and since UCR2 TXEN is
cleared, the UART Transmitter is disabled, so nothing can feed data in
the RX FIFO. Because the Receiver is still enabled, the UCR2 CTSC and
CTS bits still have effect and the CTS (RS485 DE) control is retained.
Note that in case of RS485 DE signal active low, there is no problem and
no special handling is necessary. The CTS signal defaults to HIGH, thus
the RS485 is by default set to Receive and the bus is not blocked.
Note that while there is the possibility to control CTS using GPIO with
either CTS polarity, this has the downside of not being synchronous to
the UART IP clock and thus glitchy and susceptible to slow DE switching.
Second, on boot, before the UART driver probe callback is called, the
driver core triggers pinctrl_init_done() and configures the IOMUXC to
default state. At this point, UCR1 UARTEN and UCR2 RXEN are both still
cleared, but UART CTS_B (RS485 DE) is configured as CTS function, thus
the RTS signal is pulled HIGH by the UART IP CTS circuit.
One part of the solution here is to enable UCR1 UARTEN and UCR2 RXEN and
UTS loopback in this driver probe callback, thus unblocking the CTSC and
CTS control early on. But this is still too late, since the pin control
is already configured and CTS has been pulled HIGH for a short period
of time.
When Linux kernel boots and this driver is bound, the pin control is set
to special "init" state if the state is available, and driver can switch
the "default" state afterward when ready. This state can be used to set
the CTS line as a GPIO in DT temporarily, and a GPIO hog can force such
GPIO to LOW, thus keeping the RS485 DE line LOW early on boot. Once the
driver takes over and UCR1 UARTEN and UCR2 RXEN and UTS loopback are all
enabled, the driver can switch to "default" pin control state and control
the CTS line as function instead. DT binding example is below:
"
&gpio6 {
rts-init-hog {
gpio-hog;
gpios = <5 0>;
output-low;
line-name = "rs485-de";
};
};
&uart5 { /* DHCOM UART2 */
pinctrl-0 = <&pinctrl_uart5>;
pinctrl-1 = <&pinctrl_uart5_init>;
pinctrl-names = "default", "init";
...
};
pinctrl_uart5_init: uart5-init-grp {
fsl,pins = <
...
MX6QDL_PAD_CSI0_DAT19__GPIO6_IO05 0x30b1
>;
};
pinctrl_uart5: uart5-grp {
fsl,pins = <
...
MX6QDL_PAD_CSI0_DAT19__UART5_CTS_B 0x30b1
>;
};
"
Tested-by: Christoph Niedermaier <cniedermaier@dh-electronics.com>
Reviewed-by: Fabio Estevam <festevam@denx.de>
Signed-off-by: Marek Vasut <marex@denx.de>
Link: https://lore.kernel.org/r/20220929144400.13571-1-marex@denx.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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JZ4750/55/60 (but not JZ4760b) have an optional /2 divider between the
EXT oscillator and some peripherals including UART, which will
be enabled if using a 24 MHz oscillator, and disabled when
using a 12 MHz oscillator.
This behavior relies on hardware differences: most boards (if not all)
with those SoCs have 12 or 24 MHz oscillators but many peripherals want
12Mhz to operate properly (AIC and USB-PHY at least).
The 16MHz threshold looks arbitrary but used in vendor's bootloader code
for enable the divider.
The patch doesn't affect JZ4760's behavior as it is subject for another
patchset with re-classification of all supported ingenic UARTs.
Link: https://github.com/carlos-wong/uboot_jz4755/blob/master/cpu/mips/jz_serial.c#L158
Signed-off-by: Siarhei Volkau <lis8215@gmail.com>
Link: https://lore.kernel.org/r/20221031184041.1338129-3-lis8215@gmail.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Read the DMA status before terminating the DMA, as doing so deletes
the DMA desc.
Also, to get the correct transfer status information, pause the DMA
using dmaengine_pause() before reading the DMA status.
Fixes: e9ea096dd225 ("serial: tegra: add serial driver")
Reviewed-by: Jon Hunter <jonathanh@nvidia.com>
Reviewed-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Acked-by: Thierry Reding <treding@nvidia.com>
Signed-off-by: Akhil R <akhilrajeev@nvidia.com>
Signed-off-by: Kartik <kkartik@nvidia.com>
Link: https://lore.kernel.org/r/1666105086-17326-1-git-send-email-kkartik@nvidia.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Take advantage of the new uart_xmit_advance() helper.
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20221019091151.6692-45-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Take advantage of the new uart_xmit_advance() helper.
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20221019091151.6692-44-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Take advantage of the new uart_xmit_advance() helper.
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20221019091151.6692-43-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Take advantage of the new uart_xmit_advance() helper.
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20221019091151.6692-42-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Take advantage of the new uart_xmit_advance() helper.
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20221019091151.6692-41-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Take advantage of the new uart_xmit_advance() helper.
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20221019091151.6692-40-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Take advantage of the new uart_xmit_advance() helper.
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20221019091151.6692-39-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Take advantage of the new uart_xmit_advance() helper.
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20221019091151.6692-38-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Take advantage of the new uart_xmit_advance() helper.
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20221019091151.6692-37-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Take advantage of the new uart_xmit_advance() helper.
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20221019091151.6692-36-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Take advantage of the new uart_xmit_advance() helper.
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20221019091151.6692-35-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Take advantage of the new uart_xmit_advance() helper.
Reviewed-by: Baolin Wang <baolin.wang@linux.alibaba.com>
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20221019091151.6692-34-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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