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* Merge git://git.kernel.org/pub/scm/linux/kernel/git/davem/sparc-nextLinus Torvalds2012-01-091-2/+2
|\ | | | | | | | | | | | | | | | | | | | | * git://git.kernel.org/pub/scm/linux/kernel/git/davem/sparc-next: sparc32: remove unused file: include/asm/pgtsun4.h sparc32: fix PAGE_SIZE definition sparc32: enable different preemptions models sparc32: support atomic64_t apbuart: fix section mismatch warning sparc32: drop useless preprocessor conditional in atomic_32.h sparc32: drop unused atomic24 support
| * apbuart: fix section mismatch warningSam Ravnborg2011-12-271-2/+2
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Fix following warnings: WARNING: drivers/tty/serial/built-in.o(.text+0x7370): Section mismatch in reference from the function grlib_apbuart_configure() to the variable .init.data:apbuart_match The function grlib_apbuart_configure() references the variable __initdata apbuart_match. This is often because grlib_apbuart_configure lacks a __initdata annotation or the annotation of apbuart_match is wrong. + 3 more warnings like this. There is no guarantee that grlib_apbuart_of_driver.of_match_table is only used at __init time - so drop the __initdata annotation. grlib_apbuart_configure() is only used during __init so add __init to this method too. Signed-off-by: Sam Ravnborg <sam@ravnborg.org> Cc: Daniel Hellstrom <daniel@gaisler.com> Cc: Greg Kroah-Hartman <gregkh@suse.de> Signed-off-by: David S. Miller <davem@davemloft.net>
* | Merge git://git.kernel.org/pub/scm/linux/kernel/git/davem/netLinus Torvalds2012-01-0910-13/+11
|\ \ | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | * git://git.kernel.org/pub/scm/linux/kernel/git/davem/net: igmp: Avoid zero delay when receiving odd mixture of IGMP queries netdev: make net_device_ops const bcm63xx: make ethtool_ops const usbnet: make ethtool_ops const net: Fix build with INET disabled. net: introduce netif_addr_lock_nested() and call if when appropriate net: correct lock name in dev_[uc/mc]_sync documentations. net: sk_update_clone is only used in net/core/sock.c 8139cp: fix missing napi_gro_flush. pktgen: set correct max and min in pktgen_setup_inject() smsc911x: Unconditionally include linux/smscphy.h in smsc911x.h asix: fix infinite loop in rx_fixup() net: Default UDP and UNIX diag to 'n'. r6040: fix typo in use of MCR0 register bits net: fix sock_clone reference mismatch with tcp memcontrol
| * | netdev: make net_device_ops conststephen hemminger2012-01-092-3/+2
| | | | | | | | | | | | | | | | | | | | | More drivers where net_device_ops should be const. Signed-off-by: Stephen Hemminger <shemminger@vyatta.com> Signed-off-by: David S. Miller <davem@davemloft.net>
| * | bcm63xx: make ethtool_ops conststephen hemminger2012-01-091-1/+1
| | | | | | | | | | | | | | | Signed-off-by: Stephen Hemminger <shemminger@vyatta.com> Signed-off-by: David S. Miller <davem@davemloft.net>
| * | usbnet: make ethtool_ops conststephen hemminger2012-01-094-5/+5
| | | | | | | | | | | | | | | | | | | | | | | | The ethtool_ops table of function pointers should be const. Fix all the usb network drivers. Signed-off-by: Stephen Hemminger <shemminger@vyatta.com> Signed-off-by: David S. Miller <davem@davemloft.net>
| * | 8139cp: fix missing napi_gro_flush.françois romieu2012-01-091-0/+1
| | | | | | | | | | | | | | | | | | | | | | | | | | | The driver uses __napi_complete and napi_gro_receive. Without it, the driver hits the BUG_ON(n->gro_list) assertion hard in __napi_complete. Signed-off-by: Francois Romieu <romieu@fr.zoreil.com> Tested-by: Marin Glibic <zhilla2@gmail.com> Signed-off-by: David S. Miller <davem@davemloft.net>
| * | smsc911x: Unconditionally include linux/smscphy.h in smsc911x.hDavid S. Miller2012-01-071-2/+0
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | The energy detect enable/disable code in the driver uses some register defines in this header unconditionally, so guarding the smscphy.h header include with CONFIG_SMSC_PHY leads to build failures in some configurations. Reported-by: Shawn Guo <shawn.guo@linaro.org> Signed-off-by: David S. Miller <davem@davemloft.net>
| * | asix: fix infinite loop in rx_fixup()Aurelien Jacobs2012-01-071-1/+1
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | At this point if skb->len happens to be 2, the subsequant skb_pull(skb, 4) call won't work and the skb->len won't be decreased and won't ever reach 0, resulting in an infinite loop. With an ASIX 88772 under heavy load, without this patch, rx_fixup() reaches an infinite loop in less than a minute. With this patch applied, no infinite loop even after hours of heavy load. Signed-off-by: Aurelien Jacobs <aurel@gnuage.org> Signed-off-by: David S. Miller <davem@davemloft.net>
| * | r6040: fix typo in use of MCR0 register bitsCesar Eduardo Barros2012-01-071-1/+1
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Commit 4e16d6ebd65b4f2c4e3f780b4c5704beef64019c (r6040: define more MCR0 register bits) added #define values for MCR0 register bits and converted uses of hardcoded magic values to uses of these defines. However, one of the conversions looks suspicious: #define MCR0 0x00 /* Control register 0 */ +#define MCR0_RCVEN 0x0002 /* Receive enable */ +#define MCR0_XMTEN 0x1000 /* Transmission enable */ /* Init RDC private data */ - lp->mcr0 = 0x1002; + lp->mcr0 = MCR0_XMTEN | MCR0; I believe what was meant here was MCR0_XMTEN | MCR0_RCVEN, which makes sense and matches the original values. Signed-off-by: Cesar Eduardo Barros <cesarb@cesarb.net> Signed-off-by: David S. Miller <davem@davemloft.net>
* | | Merge tag 'clk' of git://git.kernel.org/pub/scm/linux/kernel/git/arm/arm-socLinus Torvalds2012-01-098-33/+36
|\ \ \ | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | clock management changes for i.MX Another simple series related to clock management, this time only for imx. * tag 'clk' of git://git.kernel.org/pub/scm/linux/kernel/git/arm/arm-soc: ARM: mxs: select HAVE_CLK_PREPARE for clock clk: add config option HAVE_CLK_PREPARE into Kconfig ASoC: mxs-saif: convert to clk_prepare/clk_unprepare video: mxsfb: convert to clk_prepare/clk_unprepare serial: mxs-auart: convert to clk_prepare/clk_unprepare net: flexcan: convert to clk_prepare/clk_unprepare mtd: gpmi-lib: convert to clk_prepare/clk_unprepare mmc: mxs-mmc: convert to clk_prepare/clk_unprepare dma: mxs-dma: convert to clk_prepare/clk_unprepare net: fec: add clk_prepare/clk_unprepare ARM: mxs: convert platform code to clk_prepare/clk_unprepare clk: add helper functions clk_prepare_enable and clk_disable_unprepare Fix up trivial conflicts in drivers/net/ethernet/freescale/fec.c due to commit 0ebafefcaa7a ("net: fec: add clk_prepare/clk_unprepare") clashing trivially with commit e163cc97f9ac ("net/fec: fix the .remove code").
| * \ \ Merge branch 'mxs/clk-prepare' of ↵Arnd Bergmann2012-01-038-33/+36
| |\ \ \ | | | | | | | | | | | | | | | git://git.linaro.org/people/shawnguo/linux-2.6 into imx/clk
| | * | | clk: add config option HAVE_CLK_PREPARE into KconfigShawn Guo2011-12-281-0/+3
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | The commit 40d3e0f (clk: provide prepare/unprepare functions) provides the config option HAVE_CLK_PREPARE for platforms that have prepare/unprepare implementation to select. This patch adds the option into drivers/clk/Kconfig, so that it can be actually selected. Signed-off-by: Shawn Guo <shawn.guo@linaro.org> Cc: Russell King <rmk+kernel@arm.linux.org.uk>
| | * | | video: mxsfb: convert to clk_prepare/clk_unprepareShawn Guo2011-12-281-4/+4
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | The patch converts mxsfb driver to clk_prepare/clk_unprepare by using helper functions clk_prepare_enable/clk_disable_unprepare. Signed-off-by: Shawn Guo <shawn.guo@linaro.org> Cc: Sascha Hauer <s.hauer@pengutronix.de> Acked-by: Marek Vasut <marek.vasut@gmail.com> Acked-by: Florian Tobias Schandinat <FlorianSchandinat@gmx.de>
| | * | | serial: mxs-auart: convert to clk_prepare/clk_unprepareShawn Guo2011-12-281-4/+4
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | The patch converts mxs-auart driver to clk_prepare/clk_unprepare by using helper functions clk_prepare_enable/clk_disable_unprepare. Signed-off-by: Shawn Guo <shawn.guo@linaro.org> Cc: Sascha Hauer <s.hauer@pengutronix.de> Cc: Alan Cox <alan@linux.intel.com>
| | * | | net: flexcan: convert to clk_prepare/clk_unprepareShawn Guo2011-12-281-5/+5
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | The patch converts flexcan driver to clk_prepare/clk_unprepare by using helper functions clk_prepare_enable/clk_disable_unprepare. Signed-off-by: Shawn Guo <shawn.guo@linaro.org> Cc: Marc Kleine-Budde <mkl@pengutronix.de> Cc: David S. Miller <davem@davemloft.net>
| | * | | mtd: gpmi-lib: convert to clk_prepare/clk_unprepareShawn Guo2011-12-281-6/+6
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | The patch converts gpmi nand driver to clk_prepare/clk_unprepare by using helper functions clk_prepare_enable/clk_disable_unprepare. Signed-off-by: Shawn Guo <shawn.guo@linaro.org> Cc: Huang Shijie <b32955@freescale.com> Cc: Artem Bityutskiy <artem.bityutskiy@intel.com> Acked-by: Marek Vasut <marek.vasut@gmail.com>
| | * | | mmc: mxs-mmc: convert to clk_prepare/clk_unprepareShawn Guo2011-12-281-5/+5
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | The patch converts mxs-mmc driver to clk_prepare/clk_unprepare by using helper functions clk_prepare_enable/clk_disable_unprepare. Signed-off-by: Shawn Guo <shawn.guo@linaro.org> Cc: Chris Ball <cjb@laptop.org> Acked-by: Marek Vasut <marek.vasut@gmail.com>
| | * | | dma: mxs-dma: convert to clk_prepare/clk_unprepareShawn Guo2011-12-281-4/+4
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | The patch converts mxs-dma driver to clk_prepare/clk_unprepare by using helper functions clk_prepare_enable/clk_disable_unprepare. Signed-off-by: Shawn Guo <shawn.guo@linaro.org> Acked-by: Marek Vasut <marek.vasut@gmail.com> Acked-by: Vinod Koul <vinod.koul@linux.intel.com>
| | * | | net: fec: add clk_prepare/clk_unprepareRichard Zhao2011-12-281-5/+5
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | It's for migrating to generic clk framework API. Signed-off-by: Richard Zhao <richard.zhao@linaro.org> Signed-off-by: Sascha Hauer <s.hauer@pengutronix.de> Signed-off-by: Shawn Guo <shawn.guo@linaro.org> Cc: David S. Miller <davem@davemloft.net> Acked-by: Marek Vasut <marek.vasut@gmail.com>
* | | | | Merge tag 'pm' of git://git.kernel.org/pub/scm/linux/kernel/git/arm/arm-socLinus Torvalds2012-01-091-61/+367
|\ \ \ \ \ | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | power management changes for omap and imx A significant part of the changes for these two platforms went into power management, so they are split out into a separate branch. * tag 'pm' of git://git.kernel.org/pub/scm/linux/kernel/git/arm/arm-soc: (65 commits) ARM: imx6: remove __CPUINIT annotation from v7_invalidate_l1 ARM: imx6: fix v7_invalidate_l1 by adding I-Cache invalidation ARM: imx6q: resume PL310 only when CACHE_L2X0 defined ARM: imx6q: build pm code only when CONFIG_PM selected ARM: mx5: use generic irq chip pm interface for pm functions on ARM: omap: pass minimal SoC/board data for UART from dt arm/dts: Add minimal device tree support for omap2420 and omap2430 omap-serial: Add minimal device tree support omap-serial: Use default clock speed (48Mhz) if not specified omap-serial: Get rid of all pdev->id usage ARM: OMAP2+: hwmod: Add a new flag to handle hwmods left enabled at init ARM: OMAP4: PRM: use PRCM interrupt handler ARM: OMAP3: pm: use prcm chain handler ARM: OMAP: hwmod: add support for selecting mpu_irq for each wakeup pad ARM: OMAP2+: mux: add support for PAD wakeup interrupts ARM: OMAP: PRCM: add suspend prepare / finish support ARM: OMAP: PRCM: add support for chain interrupt handler ARM: OMAP3/4: PRM: add functions to read pending IRQs, PRM barrier ARM: OMAP2+: hwmod: Add API to enable IO ring wakeup ARM: OMAP2+: mux: add wakeup-capable hwmod mux entries to dynamic list ...
| * | | | | Merge branch 'v3.2-rc7' into next/pmArnd Bergmann2012-01-03305-2530/+4960
| |\| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Conflicts: arch/arm/kernel/setup.c arch/arm/mach-shmobile/board-kota2.c
| * | | | | omap-serial: Add minimal device tree supportRajendra Nayak2011-12-161-3/+42
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Adapt the driver to device tree and pass minimal platform data from device tree needed for console boot. No power management features will be suppported for now since it requires more tweaks around OCP settings to toggle forceidle/noidle/smartidle bits and handling remote wakeup and dynamic muxing. Signed-off-by: Rajendra Nayak <rnayak@ti.com> Reviewed-by: Rob Herring <rob.herring@calxeda.com> Signed-off-by: Tony Lindgren <tony@atomide.com>
| * | | | | omap-serial: Use default clock speed (48Mhz) if not specifiedRajendra Nayak2011-12-161-0/+7
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Use a default clock speed of 48Mhz, instead of ending up with 0, if platforms fail to specify a valid clock speed. Signed-off-by: Rajendra Nayak <rnayak@ti.com> Reviewed-by: Rob Herring <rob.herring@calxeda.com> Signed-off-by: Tony Lindgren <tony@atomide.com>
| * | | | | omap-serial: Get rid of all pdev->id usageRajendra Nayak2011-12-161-15/+15
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | With Device tree, pdev->id would no longer be Valid. Hence get rid of all instances of its usage in the driver. Device tree support for the driver is added in subsequent patches. Signed-off-by: Rajendra Nayak <rnayak@ti.com> Reviewed-by: Rob Herring <rob.herring@calxeda.com> Signed-off-by: Tony Lindgren <tony@atomide.com>
| * | | | | ARM: OMAP2+: UART: Fix compilation/sparse warningsGovindraj.R2011-12-151-3/+4
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Fixes below compilation warning. drivers/tty/serial/omap-serial.c: In function 'serial_omap_irq': drivers/tty/serial/omap-serial.c:228:29: warning: 'ch' may be used uninitialized in this function [-Wuninitialized] Fix below sparse warning. drivers/tty/serial/omap-serial.c:392:52: warning: incorrect type in argument 2 (different signedness) drivers/tty/serial/omap-serial.c:392:52: expected int *status drivers/tty/serial/omap-serial.c:392:52: got unsigned int *<noident> Reported-by: Kevin Hilman <khilman@ti.com> Signed-off-by: Govindraj.R <govindraj.raja@ti.com> Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes) Signed-off-by: Kevin Hilman <khilman@ti.com>
| * | | | | ARM: OMAP2+: UART: Remove omap_uart_can_sleep and add pm_qosGovindraj.R2011-12-151-1/+35
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Omap_uart_can_sleep function blocks system wide low power state until uart is active remove this func and add qos requests to prevent MPU from transitioning. Keep qos request to default value which will allow MPU to transition and while uart baud rate is available calculate the latency value from the baudrate and use the same to hold constraint while uart clocks are enabled, and if uart is auto-idled the constraint is updated with default constraint value allowing MPU to transition. Qos requests are blocking notifier calls so put these requests to work queue, also the driver uses irq_safe version of runtime API's and callbacks can be called in interrupt disabled context. So to avoid warn on slow path warning while using qos update API's from runtime callbacks use the qos_work_queue. During bootup the runtime_resume call backs might not be called and runtime callback gets called only after uart is idled by setting the autosuspend timeout. So qos_request from runtime resume callback might not activated during boot if uart baudrate is calculated during bootup for console uart, so schedule the qos_work queue once we calc_latency while configuring the uart port. Flush and complete any pending qos jobs in work queue while suspending. Signed-off-by: Govindraj.R <govindraj.raja@ti.com> Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes) Signed-off-by: Kevin Hilman <khilman@ti.com>
| * | | | | ARM: OMAP2+: UART: Make the RX_TIMEOUT for DMA configurable for each UARTJon Hunter2011-12-151-7/+8
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | When using DMA there are two timeouts defined. The first timeout, rx_timeout, is really a polling rate in which software polls the DMA status to see if the DMA has finished. This is necessary for the RX side because we do not know how much data we will receive. The secound timeout, RX_TIMEOUT, is a timeout after which the DMA will be stopped if no more data is received. To make this clearer, rename rx_timeout as rx_poll_rate and rename the function serial_omap_rx_timeout() to serial_omap_rxdma_poll(). The OMAP-Serial driver defines an RX_TIMEOUT of 3 seconds that is used to indicate when the DMA for UART can be stopped if no more data is received. The value is a global definition that is applied to all instances of the UART. Each UART may be used for a different purpose and so the timeout required may differ. Make this value configurable for each UART so that this value can be optimised for power savings. Signed-off-by: Jon Hunter <jon-hunter@ti.com> Signed-off-by: Govindraj.R <govindraj.raja@ti.com> Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes) Signed-off-by: Kevin Hilman <khilman@ti.com>
| * | | | | ARM: OMAP2+: UART: Allow UART parameters to be configured from board file.Deepak K2011-12-151-5/+3
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | The following UART parameters are defined within the UART driver: 1). Whether the UART uses DMA (dma_enabled), by default set to 0 2). The size of dma buffer (set to 4096 bytes) 3). The time after which the dma should stop if no more data is received. 4). The auto suspend delay that will be passed for pm_runtime_autosuspend where uart will be disabled after timeout Different UARTs may be used for different purpose such as the console, for interfacing bluetooth chip, for interfacing to a modem chip, etc. Therefore, it is necessary to be able to customize the above settings for a given board on a per UART basis. This change allows these parameters to be configured from the board file and allows the parameters to be configured for each UART independently. If a board does not define its own custom parameters for the UARTs, then use the default parameters in the structure "omap_serial_default_info". The default parameters are defined to be the same as the current settings in the UART driver to avoid breaking the UART for any cuurnelty supported boards. By default, make all boards use the default UART parameters. Signed-off-by: Deepak K <deepak.k@ti.com> Signed-off-by: Jon Hunter <jon-hunter@ti.com> Signed-off-by: Govindraj.R <govindraj.raja@ti.com> Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes) Signed-off-by: Kevin Hilman <khilman@ti.com>
| * | | | | ARM: OMAP2+: UART: Add wakeup mechanism for omap-uartsGovindraj.R2011-12-151-0/+15
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | From the runtime callbacks enable hwmod wakeups for uart which will internally enable io-pad wakeups for uarts if they have rx-pad pins set as wakeup capabale. Use the io-ring wakeup mechanism after uart clock gating and leave the PM_WKST set for uart to default reset values cleanup the code in serial.c which was handling PM_WKST reg. Irq_chaing(PRM_DRIVER) is used to wakeup uart after uart clocks are gated using pad wakeup mechanism. Signed-off-by: Govindraj.R <govindraj.raja@ti.com> Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes) Signed-off-by: Kevin Hilman <khilman@ti.com>
| * | | | | ARM: OMAP2+: UART: Move errata handling from serial.c to omap-serialGovindraj.R2011-12-151-4/+64
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Move the errata handling mechanism from serial.c to omap-serial file and utilise the same func in driver file. Errata i202, i291 are moved to be handled with omap-serial Moving the errata macro from serial.c file to driver header file as from on errata will be handled in driver file itself. Corrected errata id from chapter reference 2.15 to errata id i291. Removed errata and dma_enabled fields from omap_uart_state struct as they are no more needed with errata handling done within omap-serial. Signed-off-by: Govindraj.R <govindraj.raja@ti.com> Acked-by: Alan Cox <alan@linux.intel.com> Acked-by: Greg Kroah-Hartman <gregkh@suse.de> Signed-off-by: Kevin Hilman <khilman@ti.com>
| * | | | | ARM: OMAP2+: UART: Get context loss count to context restoreGovindraj.R2011-12-151-2/+18
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Avoid unconditional context restore every time we gate uart clocks. Check whether context loss happened based on which we can context restore uart regs from uart_port structure. Signed-off-by: Govindraj.R <govindraj.raja@ti.com> Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes) Signed-off-by: Kevin Hilman <khilman@ti.com>
| * | | | | ARM: OMAP2+: UART: Remove uart reset function.Govindraj.R2011-12-151-0/+1
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Remove the uart reset function which is configuring the TX empty irq which can now be handled within omap-serial driver. Signed-off-by: Govindraj.R <govindraj.raja@ti.com> Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes) Signed-off-by: Kevin Hilman <khilman@ti.com>
| * | | | | ARM: OMAP2+: UART: Ensure all reg values configured are available from port ↵Govindraj.R2011-12-151-17/+26
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | structure Add missing uart regs to uart_port structure which can be used in context restore. Store dll, dlh, mdr1, scr, efr, lcr, mcr reg values into uart_port structure while configuring individual port in termios function. Signed-off-by: Govindraj.R <govindraj.raja@ti.com> Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes) Signed-off-by: Kevin Hilman <khilman@ti.com>
| * | | | | ARM: OMAP2+: UART: Remove context_save and move context restore to driverGovindraj.R2011-12-151-0/+24
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Remove context save function from serial.c and move context restore function to omap-serial. Remove all regs stored in omap_uart_state for contex_save/restore, reg read write funcs used in context_save/restore, io_addresses populated for read/write funcs. Clock gating mechanism was done in serial.c and had no info on uart state thus we needed context save and restore in serial.c With runtime conversion and clock gating done within uart driver context restore can be done from regs value available from uart_omap_port structure. Signed-off-by: Govindraj.R <govindraj.raja@ti.com> Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes) Signed-off-by: Kevin Hilman <khilman@ti.com>
| * | | | | ARM: OMAP2+: UART: Add runtime pm support for omap-serial driverGovindraj.R2011-12-151-13/+109
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Adapts omap-serial driver to use pm_runtime API's. Use runtime runtime API's to handle uart clocks and obtain device_usage statics. Set runtime API's usage to irq_safe so that we can use get_sync from irq context. Auto-suspend for port specific activities and put for reg access. Moving suspend/resume hooks to dev_pm_ops structure and bind with config_suspend to avoid any compilation warning if config_suspend is disabled. By default uart autosuspend delay is set to -1 to avoid character loss if uart's are autoidled and woken up on rx pin. After boot up UART's can be autoidled by setting autosuspend delay from sysfs. echo 3000 > /sys/devices/platform/omap/omap_uart.X/power/autosuspend_delay_ms X=0,1,2,3 for UART1/2/3/4. Number of uarts available may vary across omap_soc. Also if uart is not wakeup capable we can prevent runtime autosuspend by forbiding runtime. Signed-off-by: Govindraj.R <govindraj.raja@ti.com> Acked-by: Alan Cox <alan@linux.intel.com> Acked-by: Greg Kroah-Hartman <gregkh@suse.de> Signed-off-by: Kevin Hilman <khilman@ti.com>
| * | | | | ARM: OMAP2+: UART: Remove mapbase/membase fields from pdata.Govindraj.R2011-12-151-2/+8
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | The mapbase (start_address), membase(io_remap cookie) part of pdata struct omap_uart_port_info are removed as this should be derived within driver. Signed-off-by: Govindraj.R <govindraj.raja@ti.com> Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes) Signed-off-by: Kevin Hilman <khilman@ti.com>
| * | | | | ARM: OMAP2+: UART: Cleanup part of clock gating mechanism for uartGovindraj.R2011-12-151-1/+0
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Currently we use a shared irq handler to identify uart activity and then trigger a timer. By default the timeout value is zero and can be set or modified from sysfs. If there was no uart activity for the period set through sysfs, the timer will expire and call timer handler this will set a flag can_sleep using which decision to gate uart clocks can be taken. Since the clock gating mechanism is outside the uart driver, we currently use this mechanism. In preparation to runtime implementation for omap-serial driver we can cleanup this mechanism and use runtime API's to gate uart clocks. Removes the following: * timer related info from local uart_state struct * the code used to set timeout value from sysfs. * irqflags used to set shared irq handler. * un-used function omap_uart_check_wakeup. Signed-off-by: Govindraj.R <govindraj.raja@ti.com> Acked-by: Greg Kroah-Hartman <gregkh@suse.de> (for drivers/tty changes) Signed-off-by: Kevin Hilman <khilman@ti.com>
* | | | | | Merge tag 'drivers' of git://git.kernel.org/pub/scm/linux/kernel/git/arm/arm-socLinus Torvalds2012-01-0928-740/+1581
|\ \ \ \ \ \ | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Driver specific changes Again, a lot of platforms have changes in here: pxa, samsung, omap, at91, imx, ... * tag 'drivers' of git://git.kernel.org/pub/scm/linux/kernel/git/arm/arm-soc: (54 commits) ARM: sa1100: clean up of the clock support ARM: pxa: add dummy clock for sa1100-rtc RTC: sa1100: support sa1100, pxa and mmp soc families RTC: sa1100: remove redundant code of setting alarm RTC: sa1100: Clean out ost register Input: zylonite-wm97xx - replace IRQ_GPIO() with gpio_to_irq() pcmcia: pxa: replace IRQ_GPIO() with gpio_to_irq() ARM: EXYNOS: Modified files for SPI consolidation work ARM: S5P64X0: Enable SDHCI support ARM: S5P64X0: Add lookup of sdhci-s3c clocks using generic names ARM: S5P64X0: Add HSMMC setup for host Controller ARM: EXYNOS: Add USB OHCI support to ORIGEN board USB: Add Samsung Exynos OHCI diver ARM: EXYNOS: Add USB OHCI support to SMDKV310 board ARM: EXYNOS: Add USB OHCI device net: macb: fix build break with !CONFIG_OF i2c: tegra: Support DVC controller in device tree i2c: tegra: Add __devinit/exit to probe/remove net/at91_ether: use gpio_is_valid for phy IRQ line ARM: at91/net: add macb ethernet controller in 9g45/9g20 DT ...
| * \ \ \ \ \ Merge branch 'samsung/driver' into next/driversArnd Bergmann2012-01-09154-1002/+2693
| |\ \ \ \ \ \ | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Conflicts: arch/arm/mach-mxs/include/mach/common.h Pull in previous samsung conflict merges and do a trivial merge of an mxs double-add conflict. Signed-off-by: Arnd Bergmann <arnd@arndb.de>
| * \ \ \ \ \ \ Merge branch 'drivers/rtc-sa1100' into next/driversArnd Bergmann2011-12-282-118/+184
| |\ \ \ \ \ \ \ | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | * drivers/rtc-sa1100: ARM: sa1100: clean up of the clock support ARM: pxa: add dummy clock for sa1100-rtc RTC: sa1100: support sa1100, pxa and mmp soc families RTC: sa1100: remove redundant code of setting alarm RTC: sa1100: Clean out ost register Conflicts: arch/arm/mach-pxa/pxa25x.c arch/arm/mach-pxa/pxa27x.c
| | * | | | | | | RTC: sa1100: support sa1100, pxa and mmp soc familiesJett.Zhou2011-12-282-80/+178
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Since the regmap of rtc on sa1100, pxa and mmp Marvell soc families are almost the same, so re-arch the rtc-sa1100 to support them. Signed-off-by: Jett.Zhou <jtzhou@marvell.com> Acked-by: Arnd Bergmann <arnd@arndb.de> Acked-by: Haojian Zhuang <haojian.zhuang@gmail.com> Acked-by: Robert Jarzmik <robert.jarzmik@free.fr> Signed-off-by: Arnd Bergmann <arnd@arndb.de>
| | * | | | | | | RTC: sa1100: remove redundant code of setting alarmJett.Zhou2011-12-281-41/+12
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | In rtc generic interface of setting alarm, it will check the alarm time value valid or not, so rtc_periodic_alarm is redundant, remove it. Signed-off-by: Jett.Zhou <jtzhou@marvell.com> Acked-by: Haojian Zhuang <haojian.zhuang@gmail.com> Signed-off-by: Arnd Bergmann <arnd@arndb.de>
| | * | | | | | | RTC: sa1100: Clean out ost registerJett.Zhou2011-12-281-3/+0
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | These registers are used in old ioctl of UIE and PIE, now they are emulated by rtc generic code of hrtimer, so it can be removed. Signed-off-by: Jett.Zhou <jtzhou@marvell.com> Acked-by: Haojian Zhuang <haojian.zhuang@gmail.com> Signed-off-by: Arnd Bergmann <arnd@arndb.de>
| * | | | | | | | Merge branch 'drivers/pxa-gpio' into next/driversArnd Bergmann2011-12-287-14/+21
| |\ \ \ \ \ \ \ \ | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | * drivers/pxa-gpio: Input: zylonite-wm97xx - replace IRQ_GPIO() with gpio_to_irq() pcmcia: pxa: replace IRQ_GPIO() with gpio_to_irq()
| | * | | | | | | | Input: zylonite-wm97xx - replace IRQ_GPIO() with gpio_to_irq()Axel Lin2011-12-281-2/+3
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Since commit 6384fd "ARM: pxa: rename IRQ_GPIO to PXA_GPIO_TO_IRQ", I got below buid errors due to implicit declaration of function 'IRQ_GPIO'. Use common gpio_to_irq() to replace machine dependant macro IRQ_GPIO(). CC drivers/input/touchscreen/zylonite-wm97xx.o drivers/input/touchscreen/zylonite-wm97xx.c: In function 'zylonite_wm97xx_probe': drivers/input/touchscreen/zylonite-wm97xx.c:195: error: implicit declaration of function 'IRQ_GPIO' make[3]: *** [drivers/input/touchscreen/zylonite-wm97xx.o] Error 1 make[2]: *** [drivers/input/touchscreen] Error 2 make[1]: *** [drivers/input] Error 2 make: *** [drivers] Error 2 Cc: Mark Brown <broonie@opensource.wolfsonmicro.com> Cc: Haojian Zhuang <haojian.zhuang@marvell.com> Signed-off-by: Axel Lin <axel.lin@gmail.com> Signed-off-by: Arnd Bergmann <arnd@arndb.de>
| | * | | | | | | | pcmcia: pxa: replace IRQ_GPIO() with gpio_to_irq()Axel Lin2011-12-286-12/+18
| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Since commit 6384fd "ARM: pxa: rename IRQ_GPIO to PXA_GPIO_TO_IRQ", I got buid errors due to implicit declaration of function 'IRQ_GPIO'. Use common gpio_to_irq() to replace machine dependant macro IRQ_GPIO(). Cc: Marek Vasut <marek.vasut@gmail.com> Cc: Ian Molton <spyro@f2s.com> Cc: Jonathan Cameron <jic23@cam.ac.uk> Cc: Zhuang <haojian.zhuang@marvell.com> Cc: Eric Miao <eric.y.miao@gmail.com> Cc: Russell King <linux@arm.linux.org.uk> Signed-off-by: Axel Lin <axel.lin@gmail.com> Acked-by: Haojian Zhuang <haojian.zhuang@gmail.com> Acked-by: Eric Miao <eric.y.miao@gmail.com> Acked-by: Marek Vasut <marek.vasut@gmail.com> Signed-off-by: Arnd Bergmann <arnd@arndb.de>
| * | | | | | | | | Merge branch 'samsung/cleanup' into next/driversArnd Bergmann2011-12-2815-1145/+712
| |\ \ \ \ \ \ \ \ \ | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | Dependency for the samsung/drivers branch Conflicts: arch/arm/mach-exynos/Makefile Signed-off-by: Arnd Bergmann <arnd@arndb.de>
| * \ \ \ \ \ \ \ \ \ Merge branch 'samsung/ohci' into next/driversArnd Bergmann2011-12-284-0/+286
| |\ \ \ \ \ \ \ \ \ \ | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | * samsung/ohci: ARM: EXYNOS: Add USB OHCI support to ORIGEN board USB: Add Samsung Exynos OHCI diver ARM: EXYNOS: Add USB OHCI support to SMDKV310 board ARM: EXYNOS: Add USB OHCI device
| | * | | | | | | | | | USB: Add Samsung Exynos OHCI diverJingoo Han2011-12-234-0/+286
| | | |_|_|_|_|_|/ / / | | |/| | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | | This patch adds USB OHCI driver for Samsung EXYNOS SoCs. Signed-off-by: Jingoo Han <jg1.han@samsung.com> Acked-by: Greg Kroah-Hartman <gregkh@suse.de> Signed-off-by: Kukjin Kim <kgene.kim@samsung.com>